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|
Attributes | |
ACN | 1180324 |
Time | |
Date | 201406 |
Local Time Of Day | 1201-1800 |
Place | |
Locale Reference | ZZZ.Airport |
State Reference | US |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Make Model Name | EMB ERJ 190/195 ER/LR |
Operating Under FAR Part | Part 121 |
Flight Phase | Initial Climb |
Component | |
Aircraft Component | Horizontal Stabilizer Trim |
Person 1 | |
Function | Pilot Flying Captain |
Qualification | Flight Crew Air Transport Pilot (ATP) |
Experience | Flight Crew Total 20500 |
Person 2 | |
Function | Technician |
Qualification | Maintenance Powerplant Maintenance Airframe |
Experience | Maintenance Technician 16 |
Events | |
Anomaly | Aircraft Equipment Problem Critical Deviation - Procedural Published Material / Policy Deviation - Procedural FAR Inflight Event / Encounter Other / Unknown |
Narrative:
RNAV departure; pitch trimmed airplane 'up'; tried to engage autopilot at 1;000 feet MSL. Autopilot would not engage. Retrimmed pitch 'up' again; elevator trim went to full down. Declared emergency. First officer (first officer) ran QRH for pitch trim runaway. Airplane accelerated to 265 knots; disengaged autothrottles; returned to field landed on runway 17 left. Captain's pitch trim [switch on yoke] was wired backwards. [Recommend] better quality control; safety inspector.
Original NASA ASRS Text
Title: A Captain describes his efforts to regain control of an EMB190 aircraft during initial climb when the aircraft suddenly pitched 'Full Down' after he had attempted to retrim Pitch 'Up'; using the Manual Pitch Trim switch on his Control column. Aircraft had accelerated to 265 knots. Emergency declared. Two mechanics also report their involvement with replacement of the Captain's Pitch Trim switch that was later found installed backwards.
Narrative: RNAV departure; pitch trimmed airplane 'Up'; tried to engage autopilot at 1;000 feet MSL. Autopilot would not engage. Retrimmed pitch 'Up' again; Elevator Trim went to full down. Declared emergency. First Officer (FO) ran QRH for Pitch Trim runaway. Airplane accelerated to 265 knots; disengaged autothrottles; returned to field landed on Runway 17 L. Captain's Pitch Trim [switch on yoke] was wired backwards. [Recommend] better Quality Control; safety inspector.
Data retrieved from NASA's ASRS site and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.