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|
Attributes | |
ACN | 118050 |
Time | |
Date | 198907 |
Day | Mon |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : dal |
State Reference | TX |
Altitude | msl bound lower : 2000 msl bound upper : 2000 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tower : dal |
Operator | common carrier : air taxi |
Make Model Name | Small Aircraft, Low Wing, 2 Eng, Retractable Gear |
Flight Phase | cruise other landing other |
Flight Plan | VFR |
Person 1 | |
Affiliation | Other |
Function | flight crew : single pilot |
Qualification | pilot : commercial pilot : instrument |
Experience | flight time last 90 days : 340 flight time total : 1460 flight time type : 10 |
ASRS Report | 118050 |
Person 2 | |
Affiliation | Other |
Function | observation : passenger |
Qualification | pilot : private |
Events | |
Anomaly | aircraft equipment problem : critical |
Independent Detector | other flight crewa |
Resolutory Action | flight crew : overcame equipment problem flight crew : declared emergency |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Narrative:
I was delivering an small aircraft for a dealer out of tulsa, ok. Upon landing at dal was unable to get a visible green for the landing gear, made 2 approachs trying bulbs and dimming lights and felt that I had a light but only too dim to see well during the day. Upon landing I had aircraft looked at and maintenance found that there was a problem with the rheostat. Gear indicator operated normally after this. 2 hours later took a buyer for demonstration ride and upon returning to dal for landing was unable to get gear down and confirmed this both with a nacelle mirror and tower fly-by. Left pattern to ponder and correct condition. Went through emergency procedures which included disengaging gear motor and manually trying to lower gear. Found that circuit breaker out and spent approximately 30 mins reengaging gear motor. Gear was then lowered mechanically. After landing no definite answer was found, other than an awl tool was found to have been left in the gear well by a previous mechanic, however this was not proven to be the problem. This aircraft was in full compliance with all far's, as well as was PIC.
Original NASA ASRS Text
Title: PLT OF LIGHT TWIN ENGINE ACFT EXPERIENCED GEAR PROBLEMS, BUT OVERCOMES THE DIFFICULTY FOR A SAFE LNDG.
Narrative: I WAS DELIVERING AN SMA FOR A DEALER OUT OF TULSA, OK. UPON LNDG AT DAL WAS UNABLE TO GET A VISIBLE GREEN FOR THE LNDG GEAR, MADE 2 APCHS TRYING BULBS AND DIMMING LIGHTS AND FELT THAT I HAD A LIGHT BUT ONLY TOO DIM TO SEE WELL DURING THE DAY. UPON LNDG I HAD ACFT LOOKED AT AND MAINT FOUND THAT THERE WAS A PROB WITH THE RHEOSTAT. GEAR INDICATOR OPERATED NORMALLY AFTER THIS. 2 HRS LATER TOOK A BUYER FOR DEMO RIDE AND UPON RETURNING TO DAL FOR LNDG WAS UNABLE TO GET GEAR DOWN AND CONFIRMED THIS BOTH WITH A NACELLE MIRROR AND TWR FLY-BY. LEFT PATTERN TO PONDER AND CORRECT CONDITION. WENT THROUGH EMER PROCS WHICH INCLUDED DISENGAGING GEAR MOTOR AND MANUALLY TRYING TO LOWER GEAR. FOUND THAT CB OUT AND SPENT APPROX 30 MINS REENGAGING GEAR MOTOR. GEAR WAS THEN LOWERED MECHANICALLY. AFTER LNDG NO DEFINITE ANSWER WAS FOUND, OTHER THAN AN AWL TOOL WAS FOUND TO HAVE BEEN LEFT IN THE GEAR WELL BY A PREVIOUS MECH, HOWEVER THIS WAS NOT PROVEN TO BE THE PROB. THIS ACFT WAS IN FULL COMPLIANCE WITH ALL FAR'S, AS WELL AS WAS PIC.
Data retrieved from NASA's ASRS site as of August 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.