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|
Attributes | |
ACN | 1189724 |
Time | |
Date | 201407 |
Local Time Of Day | 1801-2400 |
Place | |
Locale Reference | ZZZ.Airport |
State Reference | US |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Make Model Name | B737-300 |
Operating Under FAR Part | Part 121 |
Flight Phase | Parked |
Component | |
Aircraft Component | Turbine Engine |
Person 1 | |
Function | First Officer |
Experience | Flight Crew Last 90 Days 231 Flight Crew Type 231 |
Person 2 | |
Function | Captain |
Qualification | Flight Crew Air Transport Pilot (ATP) |
Experience | Flight Crew Last 90 Days 174 |
Events | |
Anomaly | Aircraft Equipment Problem Critical Deviation - Procedural Published Material / Policy |
Narrative:
Our originating flight was delayed over four hours out of ZZZ. Company maintenance was working the problem of a fuel leak on the number 2 (right) engine. Company maintenance signed-off the leak as 'within limits' on the [log] page prior to the contract maintenance write-up stating that the leak was out of limits. We questioned the mechanic about the seemingly backwards write-up; and were told that it was satisfactory. Upon arriving at ZZZ1; the engine was still leaking and maintenance informed us that the write-up was not satisfactory and the aircraft was taken out of service. [Recommend to] double check with maintenance control if you have questions. Improper mechanic logbook sign-off.
Original NASA ASRS Text
Title: After arrival; a Captain and First Officer were informed by Company Base Maintenance personnel that Logbook Corrective Action entries at their previous departing station for Number 2 (Right) Engine fuel leaking were incorrect and the B737-300 aircraft had to be grounded.
Narrative: Our originating flight was delayed over four hours out of ZZZ. Company Maintenance was working the problem of a fuel leak on the Number 2 (Right) Engine. Company Maintenance signed-off the leak as 'within limits' on the [Log] page prior to the Contract Maintenance write-up stating that the leak was out of limits. We questioned the Mechanic about the seemingly backwards write-up; and were told that it was satisfactory. Upon arriving at ZZZ1; the engine was still leaking and Maintenance informed us that the write-up was not satisfactory and the aircraft was taken out of service. [Recommend to] double check with Maintenance Control if you have questions. Improper Mechanic Logbook sign-off.
Data retrieved from NASA's ASRS site and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.