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|
Attributes | |
ACN | 127486 |
Time | |
Date | 198911 |
Day | Sun |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | airport : dal airport : dfw |
State Reference | TX |
Altitude | agl bound lower : 0 agl bound upper : 0 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tracon : dfw |
Operator | common carrier : air carrier |
Make Model Name | Light Transport, Low Wing, 2 Turboprop Eng |
Flight Phase | landing other other other |
Route In Use | departure other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : instrument pilot : commercial |
Experience | flight time total : 3096 |
ASRS Report | 127486 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Experience | flight time last 90 days : 200 flight time total : 4300 |
ASRS Report | 127639 |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other anomaly other |
Independent Detector | other flight crewa |
Resolutory Action | flight crew : declared emergency other |
Consequence | other |
Supplementary | |
Primary Problem | Aircraft |
Narrative:
Departed dfw via runway 17L. Takeoff roll and initial climb normal through level off at 2000'. Upon being cleared to climb to 4000' detected 'dirty socks' odor emanating from air cycle machine, followed by slight trace of blue smoke in cockpit. Further examination revealed substantial smoke emanating from cabin floor vents. Received clearance to return to dfw. Right engine oil pressure sunk to zero instantly. Performed smoke removal and emergency engine shutdown checklist procedures. Elected change in destination to love field and received clearance for same. Heavy smoke/fog in cabin. Stable on final approach. Experienced 1500 FPM sink rate at 500' AGL. Unable to arrest sink rate. Touched down on main gear brushing tail cone on runway. Bounced indeterminate height and returned to runway unable to control direction of aircraft on return to runway. Aircraft exited runway pavement and proceeded to parallel taxiway. Directional control reestablished. Shutdown procedures employed, passenger deplaned, no injuries.
Original NASA ASRS Text
Title: ACR LTT TURBOPROP EXPERIENCES SMOKE IN CABIN AND COCKPIT SHORTLY AFTER DEP FROM DFW. ACFT DIVERTS FOR EMERGENCY LNDG AT DAL WHERE THEY EXPERIENCE HARD LNDG BUT NO INJURIES.
Narrative: DEPARTED DFW VIA RWY 17L. TKOF ROLL AND INITIAL CLIMB NORMAL THROUGH LEVEL OFF AT 2000'. UPON BEING CLRED TO CLIMB TO 4000' DETECTED 'DIRTY SOCKS' ODOR EMANATING FROM AIR CYCLE MACHINE, FOLLOWED BY SLIGHT TRACE OF BLUE SMOKE IN COCKPIT. FURTHER EXAMINATION REVEALED SUBSTANTIAL SMOKE EMANATING FROM CABIN FLOOR VENTS. RECEIVED CLRNC TO RETURN TO DFW. RIGHT ENGINE OIL PRESSURE SUNK TO ZERO INSTANTLY. PERFORMED SMOKE REMOVAL AND EMER ENGINE SHUTDOWN CHECKLIST PROCS. ELECTED CHANGE IN DEST TO LOVE FIELD AND RECEIVED CLRNC FOR SAME. HEAVY SMOKE/FOG IN CABIN. STABLE ON FINAL APCH. EXPERIENCED 1500 FPM SINK RATE AT 500' AGL. UNABLE TO ARREST SINK RATE. TOUCHED DOWN ON MAIN GEAR BRUSHING TAIL CONE ON RWY. BOUNCED INDETERMINATE HEIGHT AND RETURNED TO RWY UNABLE TO CONTROL DIRECTION OF ACFT ON RETURN TO RWY. ACFT EXITED RWY PAVEMENT AND PROCEEDED TO PARALLEL TXWY. DIRECTIONAL CONTROL REESTABLISHED. SHUTDOWN PROCS EMPLOYED, PAX DEPLANED, NO INJURIES.
Data retrieved from NASA's ASRS site as of August 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.