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|
Attributes | |
ACN | 1331662 |
Time | |
Date | 201602 |
Local Time Of Day | 1201-1800 |
Place | |
Locale Reference | ZZZ.Airport |
State Reference | US |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Make Model Name | B737 Undifferentiated or Other Model |
Operating Under FAR Part | Part 121 |
Flight Phase | Parked |
Flight Plan | IFR |
Component | |
Aircraft Component | Oxygen System/Crew |
Person 1 | |
Function | Captain Pilot Flying FBO Personnel |
Qualification | Flight Crew Air Transport Pilot (ATP) |
Experience | Flight Crew Last 90 Days 125 Flight Crew Total 19000 Flight Crew Type 7103 |
Events | |
Anomaly | Aircraft Equipment Problem Less Severe Deviation - Procedural FAR Deviation - Procedural Published Material / Policy |
Narrative:
We arrived at the airplane from layover; and preformed our preflight duties. When I checked the O2; the pressure dropped approx. 400 lbs. And stayed there - recovering after the test. I asked the first officer (first officer) to test; and got the same result. We then tested at the same time; and the pressure dropped about 850 lbs. I called local ops for the mechanic; wrote it up in the maintenance (mx) log book; and sent an ACARS message to mx. When the contract mechanic showed up and I demonstrated the problem; he called mx control. They told him it was within limits. I requested to speak to the mx controller; who said to me that nothing was wrong since the pressure while testing; was still above allowable (approx. 950lbs). I explained that it was definitely not normal. That I've flown 737s for 10 years; and this has never happened before. I got the run around that it was a contract mx base and no parts; and who knows how long it would be before it could be corrected to my satisfaction. I indicated that the mechanic was here; and could inspect the system. I was particularly concerned that the valve was only partially open (bernoulli's principle). Mx control spoke again to the contract mechanic; who went below and inspected the system. He returned 5 minutes later - problem solved: the valve was less than one full turn open; and safety wired. He clipped the wire; turned the valve about 7 turns to full open; and reinstalled the safety wire. The system then tested normally.whomever worked on the O2 system did not follow procedure - possible catastrophe. The pilots who brought the plane in (and all those who flew it after the O2 was improperly worked on); either did not preflight the O2 system; or did not investigate a non-normal indication - possible catastrophe. I felt pressured by the mx control that I was writing up a nonissue - with a new captain; or weak personality - possible catastrophe.
Original NASA ASRS Text
Title: The shut-off valve on the Crew O2 Bottle was only open a small amount; therefore the O2 pressure would not recover in a timely manner.
Narrative: We arrived at the airplane from layover; and preformed our preflight duties. When I checked the O2; the pressure dropped approx. 400 lbs. and stayed there - recovering after the test. I asked the F/O (First Officer) to test; and got the same result. We then tested at the same time; and the pressure dropped about 850 lbs. I called local ops for the mechanic; wrote it up in the maintenance (MX) log book; and sent an ACARS message to MX. When the contract mechanic showed up and I demonstrated the problem; he called MX control. They told him it was within limits. I requested to speak to the MX controller; who said to me that nothing was wrong since the pressure while testing; was still above allowable (approx. 950lbs). I explained that it was definitely NOT normal. That I've flown 737s for 10 years; and this has never happened before. I got the run around that it was a contract MX base and no parts; and who knows how long it would be before it could be corrected to my satisfaction. I indicated that the mechanic was here; and could inspect the system. I was particularly concerned that the valve was only partially open (Bernoulli's principle). MX control spoke again to the contract mechanic; who went below and inspected the system. He returned 5 minutes later - problem solved: The valve was less than one full turn open; and safety wired. He clipped the wire; turned the valve about 7 turns to full open; and reinstalled the safety wire. The system then tested normally.Whomever worked on the O2 system did not follow procedure - possible catastrophe. The pilots who brought the plane in (and all those who flew it after the O2 was improperly worked on); either did not preflight the O2 system; or did not investigate a non-normal indication - possible catastrophe. I felt pressured by the MX control that I was writing up a nonissue - With a new captain; or weak personality - possible catastrophe.
Data retrieved from NASA's ASRS site and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.