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|
Attributes | |
ACN | 1374049 |
Time | |
Date | 201607 |
Local Time Of Day | 1801-2400 |
Place | |
Locale Reference | ZZZ.Airport |
State Reference | US |
Environment | |
Light | Daylight |
Aircraft 1 | |
Make Model Name | Cessna 402/402C/B379 Businessliner/Utiliner |
Flight Phase | Climb |
Flight Plan | IFR |
Component | |
Aircraft Component | Reciprocating Engine Assembly |
Person 1 | |
Function | Captain Pilot Flying |
Qualification | Flight Crew Air Transport Pilot (ATP) |
Events | |
Anomaly | Aircraft Equipment Problem Critical Inflight Event / Encounter Fuel Issue |
Narrative:
We had just taken off and I was making a power reduction and when pulling back the mixture the fuel flow went below normal; 74 lb/hr the first officer asked what I was doing. I thought I had pulled it back too far and advanced the mixture a half inch thinking this would reverse the trend. It helped momentarily but then the fuel flow went back down. So I pushed the mixture farther forward. At this point the engine staggered. I went full forward on the mixture the engine now quit completely. The first officer announced 'no fuel flow; this is a failure.' I immediately went through the red box items and when turning the pump to high the engine came back to life. I flew and gave the first officer the QRH he went through it. I called approach and told them we needed to come back. We landed with no further problems.
Original NASA ASRS Text
Title: C402 Captain experienced a momentary engine failure while attempting to adjust the mixture after takeoff. When the fuel pump was turned too high the engine came back to life. The crew elected to return to the departure airport.
Narrative: We had just taken off and I was making a power reduction and when pulling back the mixture the fuel flow went below normal; 74 lb/hr The First Officer asked what I was doing. I thought I had pulled it back too far and advanced the mixture a half inch thinking this would reverse the trend. It helped momentarily but then the fuel flow went back down. So I pushed the mixture farther forward. At this point the engine staggered. I went full forward on the mixture the engine now quit completely. The First Officer announced 'no fuel flow; this is a failure.' I immediately went through the red box items and when turning the pump to high the engine came back to life. I flew and gave the First Officer the QRH he went through it. I called approach and told them we needed to come back. We landed with no further problems.
Data retrieved from NASA's ASRS site and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.