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|
Attributes | |
ACN | 1383939 |
Time | |
Date | 201608 |
Local Time Of Day | 0601-1200 |
Place | |
Locale Reference | ZZZ.TRACON |
State Reference | US |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Make Model Name | M-20 K (231) / Encore |
Operating Under FAR Part | Part 91 |
Flight Phase | Cruise |
Flight Plan | VFR |
Component | |
Aircraft Component | Engine |
Person 1 | |
Function | Pilot Flying Single Pilot |
Qualification | Flight Crew Private |
Experience | Flight Crew Last 90 Days 73 Flight Crew Total 767 Flight Crew Type 3 |
Events | |
Anomaly | Aircraft Equipment Problem Critical Ground Event / Encounter Ground Strike - Aircraft |
Narrative:
During a test flight of a newly purchased airplane within 5 to 7 minutes after takeoff I experienced two quick pops from the engine. Within 3 seconds of engine popping; the engine quit. I turned on the low boost pump and switched fuel tanks. The engine was still popping and making 20% power to 0% power. I held the high boost pump to the on position and the engine would make a bit more power; however was still losing altitude. After reaching 800 feet AGL picked a suitable off field landing. Set the airplane up with flaps/trim and gear down and committed to my off field landing. After coming to a stop and exiting the airplane; noticed a blue streak of liquid down the left-side of fuselage. Raised oil fill door on top of engine cowling and noticed strong fuel odor. Upon further inspection; found a 1/4 inch fuel line disconnected on fuel system.
Original NASA ASRS Text
Title: M20K pilot reported landing in a field after the engine quit in flight. Inspection on the ground revealed a fuel line had become disconnected.
Narrative: During a test flight of a newly purchased airplane within 5 to 7 minutes after takeoff I experienced two quick pops from the engine. Within 3 seconds of engine popping; the engine quit. I turned on the low boost pump and switched fuel tanks. The engine was still popping and making 20% power to 0% power. I held the high boost pump to the on position and the engine would make a bit more power; however was still losing altitude. After reaching 800 feet AGL picked a suitable off field landing. Set the airplane up with flaps/trim and gear down and committed to my off field landing. After coming to a stop and exiting the airplane; noticed a blue streak of liquid down the left-side of fuselage. Raised oil fill door on top of engine cowling and noticed strong fuel odor. Upon further inspection; found a 1/4 inch fuel line disconnected on fuel system.
Data retrieved from NASA's ASRS site and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.