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|
Attributes | |
ACN | 149095 |
Time | |
Date | 199006 |
Day | Thu |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : bed |
State Reference | MA |
Altitude | msl bound lower : 1500 msl bound upper : 2200 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tower : bed |
Operator | common carrier : air taxi |
Make Model Name | Helicopter |
Flight Phase | cruise other descent other |
Route In Use | approach : visual arrival other |
Flight Plan | VFR |
Person 1 | |
Affiliation | Other |
Function | flight crew : single pilot |
Qualification | pilot : private pilot : instrument pilot : commercial pilot : cfi |
Experience | flight time last 90 days : 90 flight time total : 4500 flight time type : 800 |
ASRS Report | 149095 |
Person 2 | |
Affiliation | government : faa |
Function | controller : local |
Qualification | controller : non radar |
Events | |
Anomaly | aircraft equipment problem : critical non adherence : published procedure |
Independent Detector | other flight crewa |
Resolutory Action | none taken : detected after the fact |
Consequence | Other |
Supplementary | |
Primary Problem | Ambiguous |
Air Traffic Incident | other other |
Narrative:
After washing helicopter and preflting, I departed minuteman airfield at am:50 for our boxboro helipad. I had our agent load 3 passenger. I departed boxboro at am:00 for burlington. At approximately am:12 I was descending out of 2200' MSL when the aircraft began to shake. At 1500' MSL, roughly 15 seconds, a loud bang was heard and the helicopter stopped shaking. During the shaking my attention was inside the aircraft for any sign of engine or transmission problems. All indications were fine. I was already in a descent with my helipad in sight. I continued to the pad where I got out to board my passenger. As I looked at the helicopter, it was very apparent that the pilot side engine cowling had departed the aircraft. I shut down and called maintenance.
Original NASA ASRS Text
Title: ROTARY WINGED ACFT LOSES ENGINE COWLING WHILE DESCENDING TO HELIPAD ON FIRST FLT OF THE DAY.
Narrative: AFTER WASHING HELI AND PREFLTING, I DEPARTED MINUTEMAN AIRFIELD AT AM:50 FOR OUR BOXBORO HELIPAD. I HAD OUR AGENT LOAD 3 PAX. I DEPARTED BOXBORO AT AM:00 FOR BURLINGTON. AT APPROX AM:12 I WAS DSNDING OUT OF 2200' MSL WHEN THE ACFT BEGAN TO SHAKE. AT 1500' MSL, ROUGHLY 15 SECS, A LOUD BANG WAS HEARD AND THE HELI STOPPED SHAKING. DURING THE SHAKING MY ATTN WAS INSIDE THE ACFT FOR ANY SIGN OF ENG OR XMISSION PROBS. ALL INDICATIONS WERE FINE. I WAS ALREADY IN A DSNT WITH MY HELIPAD IN SIGHT. I CONTINUED TO THE PAD WHERE I GOT OUT TO BOARD MY PAX. AS I LOOKED AT THE HELI, IT WAS VERY APPARENT THAT THE PLT SIDE ENG COWLING HAD DEPARTED THE ACFT. I SHUT DOWN AND CALLED MAINT.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.