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|
Attributes | |
ACN | 160506 |
Time | |
Date | 199010 |
Day | Mon |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | atc facility : djb |
State Reference | OH |
Altitude | msl bound lower : 7000 msl bound upper : 7000 |
Environment | |
Flight Conditions | IMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tracon : cle |
Operator | common carrier : air carrier |
Make Model Name | Small Transport, Low Wing, 2 Turboprop Eng |
Flight Phase | cruise other other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Experience | flight time last 90 days : 195 flight time total : 6245 flight time type : 195 |
ASRS Report | 160506 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : commercial pilot : instrument |
Events | |
Anomaly | aircraft equipment problem : critical |
Independent Detector | aircraft equipment other aircraft equipment : unspecified other flight crewa |
Resolutory Action | flight crew : declared emergency other |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Narrative:
Over tvt at 15000' MSL, noted left engine oil pressure fluctuating 50-70 psi. Initiated descent with cle center to 11000' MSL with possible engine shutdown with first officer. During approach phase at 7000' MSL, left engine oil pressure dropped to 5-10 psi with propeller starting to surge. Precautionary engine shutdown accomplished and emergency declared with cle approach. Flew ASR to 5R. Cleared by tower to land 5L. Landed with no further complications. Aircraft nose wheel steering inoperative, and could not make right turns to clear taxiway between 5L and 5R. Passenger (13) deplaned to bus. Aircraft towed to maintenance with no further complications. Post-flight showed oil tank empty with oil leaking out of cowling. Engine reserviced with oil. Found propeller government pressure relief line leaking at lower b-nut. Oil line replaced, engine serviced and run. Corrected discrepancy. Aircraft ferried to mob.
Original NASA ASRS Text
Title: COMMUTER SMT FLT CREW EXPERIENCES OIL LOSS ON LEFT ENGINE, DIVERTS TO AN EMERGENCY LNDG WITH ENGINE SHUTDOWN.
Narrative: OVER TVT AT 15000' MSL, NOTED LEFT ENG OIL PRESSURE FLUCTUATING 50-70 PSI. INITIATED DSNT WITH CLE CENTER TO 11000' MSL WITH POSSIBLE ENG SHUTDOWN WITH F/O. DURING APCH PHASE AT 7000' MSL, LEFT ENG OIL PRESSURE DROPPED TO 5-10 PSI WITH PROP STARTING TO SURGE. PRECAUTIONARY ENG SHUTDOWN ACCOMPLISHED AND EMER DECLARED WITH CLE APCH. FLEW ASR TO 5R. CLRED BY TWR TO LAND 5L. LANDED WITH NO FURTHER COMPLICATIONS. ACFT NOSE WHEEL STEERING INOP, AND COULD NOT MAKE RIGHT TURNS TO CLR TXWY BTWN 5L AND 5R. PAX (13) DEPLANED TO BUS. ACFT TOWED TO MAINT WITH NO FURTHER COMPLICATIONS. POST-FLT SHOWED OIL TANK EMPTY WITH OIL LEAKING OUT OF COWLING. ENG RESERVICED WITH OIL. FOUND PROP GOV PRESSURE RELIEF LINE LEAKING AT LOWER B-NUT. OIL LINE REPLACED, ENG SERVICED AND RUN. CORRECTED DISCREPANCY. ACFT FERRIED TO MOB.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.