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|
Attributes | |
ACN | 1637644 |
Time | |
Date | 201904 |
Local Time Of Day | 1201-1800 |
Place | |
Locale Reference | ZZZ.Airport |
State Reference | US |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Make Model Name | B737-800 |
Operating Under FAR Part | Part 121 |
Flight Phase | Climb |
Flight Plan | IFR |
Component | |
Aircraft Component | Fuel Storage System |
Person 1 | |
Function | First Officer Pilot Not Flying |
Qualification | Flight Crew Multiengine Flight Crew Instrument Flight Crew Air Transport Pilot (ATP) |
Experience | Flight Crew Last 90 Days 187 Flight Crew Type 9832 |
Person 2 | |
Function | Pilot Flying Captain |
Qualification | Flight Crew Multiengine Flight Crew Instrument Flight Crew Air Transport Pilot (ATP) |
Experience | Flight Crew Last 90 Days 182 Flight Crew Type 11877 |
Events | |
Anomaly | Aircraft Equipment Problem Critical Deviation - Procedural Published Material / Policy Deviation - Procedural Weight And Balance Inflight Event / Encounter Fuel Issue |
Narrative:
We were reassigned last minute to this flight due to [out of duty time] timeout from previous flight block time. We both had a lot of problems getting our paperwork from pilot mobile. The flight didn't auto populate like usual; we had to manually enter the flight number; origin; and select all flight to get finally get the paper work. Upon downloading the release; we realized the prior captain has already signed for it. Captain placed a call to dispatch; and the dispatcher manually enter the required info and said it was successful. During review of the release; we both saw there was a previous write up with the right tank indicator showing 9;000 pounds. After pushback and start; we were informed fuel pouring out of the right vent. We elected to shut down and tow back to the gate. [Maintenance logbook] writeup was entered and maintenance came to test the valve. It passed the test and tank was sticked to confirm quantity. Aircraft was release for flight. During climbout; flight attendant (flight attendant) called to inform us a customer reporting fuel streaming out of the wing since initial right turn out of ZZZ. We stopped our climb and investigate. A call was placed with maintenance control. We informed them of the issue and that we were concerned with the leak; quantity; and thinking about air return. Discussion was made and maintenance said to go ahead and air return. [ATC was notified] and we landed normally slightly overweight at 148.0. Overweight landing and fuel leak writeup was entered into [logbook].
Original NASA ASRS Text
Title: B737 flight crew reported a passenger spotted fuel leaking from the wing.
Narrative: We were reassigned last minute to this flight due to [Out of Duty time] timeout from previous flight block time. We both had a lot of problems getting our paperwork from pilot mobile. The flight didn't auto populate like usual; we had to manually enter the flight number; origin; and select all flight to get finally get the paper work. Upon downloading the release; we realized the prior Captain has already signed for it. Captain placed a call to Dispatch; and the Dispatcher manually enter the required info and said it was successful. During review of the release; we both saw there was a previous write up with the right tank indicator showing 9;000 LBS. After pushback and start; we were informed fuel pouring out of the right vent. We elected to shut down and tow back to the gate. [Maintenance logbook] writeup was entered and Maintenance came to test the valve. It passed the test and tank was sticked to confirm quantity. Aircraft was release for flight. During climbout; FA (Flight Attendant) called to inform us a customer reporting fuel streaming out of the wing since initial right turn out of ZZZ. We stopped our climb and investigate. A call was placed with Maintenance control. We informed them of the issue and that we were concerned with the leak; quantity; and thinking about air return. Discussion was made and Maintenance said to go ahead and air return. [ATC was notified] and we landed normally slightly overweight at 148.0. Overweight landing and fuel leak writeup was entered into [logbook].
Data retrieved from NASA's ASRS site and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.