37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 1641869 |
Time | |
Date | 201904 |
Place | |
Locale Reference | ZZZ.Airport |
State Reference | US |
Aircraft 1 | |
Make Model Name | B757 Undifferentiated or Other Model |
Operating Under FAR Part | Part 121 |
Flight Phase | Descent |
Flight Plan | IFR |
Component | |
Aircraft Component | Rudder Control System |
Person 1 | |
Function | Captain |
Qualification | Flight Crew Instrument Flight Crew Air Transport Pilot (ATP) Flight Crew Multiengine |
Experience | Flight Crew Last 90 Days 171 Flight Crew Type 561 |
Events | |
Anomaly | Aircraft Equipment Problem Critical Deviation - Procedural Published Material / Policy |
Narrative:
This jet required 5 units of left rudder trim in level flight. It also required multiple rudder trim adjustments on approach. We wrote this up; and the jet was taken out of service. It was out of service for about three days.turns out the rudder was out of rig; the rudder ratio changer had to be replaced; there was a damaged shear pin in the original rudder ratio changer; the rudder ratio changer input rod had a broken bearing; and the control rod for the upper rudder power control actuator had a broken nut plate and frozen bolt. At least I think that's what happened -- the maintenance history is a little hard to follow -- especially since we no longer have access to the [electronic] logbook!I don't know how long it had been flying around like this; but I wanted to give this some visibility via [safety report] because flight control system malfunctions are rare; at least in my experience. A malfunctioning rudder ratio changer; in the right failure mode; could potentially be catastrophic.
Original NASA ASRS Text
Title: B757 Captain reported excessive rudder trim inputs were needed during flight.
Narrative: This jet required 5 units of left rudder trim in level flight. It also required multiple rudder trim adjustments on approach. We wrote this up; and the jet was taken out of service. It was out of service for about three days.Turns out the rudder was out of rig; the rudder ratio changer had to be replaced; there was a damaged shear pin in the original rudder ratio changer; the rudder ratio changer input rod had a broken bearing; and the control rod for the upper rudder power control actuator had a broken nut plate and frozen bolt. At least I think that's what happened -- the maintenance history is a little hard to follow -- especially since we no longer have access to the [electronic] logbook!I don't know how long it had been flying around like this; but I wanted to give this some visibility via [safety report] because flight control system malfunctions are rare; at least in my experience. A malfunctioning rudder ratio changer; in the right failure mode; could potentially be catastrophic.
Data retrieved from NASA's ASRS site and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.