37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 1703585 |
Time | |
Date | 201911 |
Local Time Of Day | 1201-1800 |
Place | |
Locale Reference | ZZZ.Airport |
State Reference | US |
Environment | |
Flight Conditions | Marginal |
Light | Night |
Aircraft 1 | |
Make Model Name | EMB ERJ 145 ER/LR |
Operating Under FAR Part | Part 121 |
Flight Phase | Climb |
Flight Plan | IFR |
Component | |
Aircraft Component | Horizontal Stabilizer Trim |
Person 1 | |
Function | Captain Pilot Flying |
Qualification | Flight Crew Air Transport Pilot (ATP) Flight Crew Multiengine |
Experience | Flight Crew Last 90 Days 177 Flight Crew Total 2800 Flight Crew Type 1500 |
Events | |
Anomaly | Aircraft Equipment Problem Critical Inflight Event / Encounter Loss Of Aircraft Control |
Narrative:
This was our third leg in the aircraft for the day and the previous crew reported no abnormalities. ZZZ was reporting windshear at 2;000 feet at 45 knots with surface winds below 10 knots in the same direction. Due to the windshear we conducted a takeoff-1 takeoff with the engine anti-ice on. The takeoff roll was normal; at 400 feet I called for heading and then yaw damper at 500 feet. At 1;000 feet I called for speed 210; and then began to trim the nose down to 10 degrees of pitch. As I was doing this the nose was not coming below 15 degrees and the control forces were becoming stronger; to the point I had the yoke fully forward attempting to lower the nose. While I was doing this I was also attempting to pitch the trim from 8 nose up to nose down. The trim was cutting out after 3 seconds; but was not actually moving and providing insufficient trim. I attempted this 3 times and from each trim cutout the trim only moved 1 unit. As the pitch trim was barely moving and cutting out I thought there could possibly be a runaway so I held the red disconnect button and alerted the first officer that there was a flight control malfunction.while holding the red disconnect I reduced the thrust levers halfway and was finally able to lower the nose. I then tried using the primary pitch trim again and it seemed to work normally. The rest of the flight was normal and I made a maintenance write up when we landed. I explained the entire situation to the maintenance controller and made a mutually agreed upon write up in the logbook.seems to be some sort of common failure in the primary pitch trim; but only in flight with control surface resistance. I had a similar experience in [a different] aircraft the previous trip; but only my first officer had experienced it. I thought she was just struggling with the weight of the control surfaces during takeoff. I found out later that particular aircraft's pitch trim had failed on another flight afterwards.
Original NASA ASRS Text
Title: EMB-145 Captain reported a pitch trim anomaly during climbout.
Narrative: This was our third leg in the aircraft for the day and the previous crew reported no abnormalities. ZZZ was reporting windshear at 2;000 feet at 45 knots with surface winds below 10 knots in the same direction. Due to the windshear we conducted a Takeoff-1 takeoff with the engine anti-ice on. The takeoff roll was normal; at 400 feet I called for heading and then yaw damper at 500 feet. At 1;000 feet I called for speed 210; and then began to trim the nose down to 10 degrees of pitch. As I was doing this the nose was not coming below 15 degrees and the control forces were becoming stronger; to the point I had the yoke fully forward attempting to lower the nose. While I was doing this I was also attempting to pitch the trim from 8 nose up to nose down. The trim was cutting out after 3 seconds; but was not actually moving and providing insufficient trim. I attempted this 3 times and from each trim cutout the trim only moved 1 unit. As the pitch trim was barely moving and cutting out I thought there could possibly be a runaway so I held the red disconnect button and alerted the First Officer that there was a flight control malfunction.While holding the red disconnect I reduced the thrust levers halfway and was finally able to lower the nose. I then tried using the primary pitch trim again and it seemed to work normally. The rest of the flight was normal and I made a maintenance write up when we landed. I explained the entire situation to the maintenance controller and made a mutually agreed upon write up in the logbook.Seems to be some sort of common failure in the primary pitch trim; but only in flight with control surface resistance. I had a similar experience in [a different] aircraft the previous trip; but only my First Officer had experienced it. I thought she was just struggling with the weight of the control surfaces during takeoff. I found out later that particular aircraft's pitch trim had failed on another flight afterwards.
Data retrieved from NASA's ASRS site and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.