Narrative:

We had a deferred APU bleed air and did a air start at the gate then went to spot 3 and did a cross bleed start. We taxied out to runway 4L and it was my leg as pilot flying. ATC was issuing windshear loss of 15 kts. On final for runway 4R and we planned for a vr max for takeoff for the windshear. Wind was 330 gusting to 27 kts. We were cleared for takeoff I set 1.1 EPR called for set thrust. Captain set it. Check thrust. Thrust checked we were accelerating. We had not hit 100 kts. When ATC issued the reject. We rejected the takeoff. I called for the flight attendants to remain seated and we taxied off the runway to taxiway P about 3;000 ft. Down the runway. I ran the qrc and pulled the QRH. Another aircraft said they saw smoke coming from our gear so we asked [crash fire rescue] to come. Brakes hit 3 on the left side with the white box. We checked on the passengers and flight attendants. I called maintenance and they said we would have to go to the ballpark for inspection. [Software] chart showed 56 min I rounded up to 100 kts. As I know we were below that. [Crash fire rescue] could not inspect our gear because they needed us to shutdown engines which we could not do because of the inoperative APU. We taxied to the [ramp] and maintenance met us and we wrote up the reject there. We also notified dispatch and the passengers and flight attendants. The brakes went back to 0 and after shutting down the left engine; maintenance cleared us. We did a crossbleed at taxiway Y short of taxiway U and got a new release with the fuel we had; new to data and departed.

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Original NASA ASRS Text

Title: B757 flight crew reported a rejected takeoff that resulted in hot brakes and a flight delay.

Narrative: We had a deferred APU bleed air and did a air start at the gate then went to spot 3 and did a cross bleed start. We taxied out to Runway 4L and it was my leg as Pilot Flying. ATC was issuing windshear loss of 15 kts. on final for Runway 4R and we planned for a Vr max for takeoff for the windshear. Wind was 330 gusting to 27 kts. We were cleared for takeoff I set 1.1 EPR called for set thrust. Captain set it. Check thrust. Thrust checked we were accelerating. We had not hit 100 kts. when ATC issued the reject. We rejected the takeoff. I called for the flight attendants to remain seated and we taxied off the runway to Taxiway P about 3;000 ft. down the runway. I ran the QRC and pulled the QRH. Another aircraft said they saw smoke coming from our gear so we asked [Crash Fire rescue] to come. Brakes hit 3 on the left side with the white box. We checked on the passengers and flight attendants. I called Maintenance and they said we would have to go to the ballpark for inspection. [Software] chart showed 56 min I rounded up to 100 kts. as I know we were below that. [Crash Fire Rescue] could not inspect our gear because they needed us to shutdown engines which we could not do because of the inoperative APU. We taxied to the [ramp] and Maintenance met us and we wrote up the reject there. We also notified Dispatch and the passengers and flight attendants. The brakes went back to 0 and after shutting down the left engine; Maintenance cleared us. We did a crossbleed at Taxiway Y short of Taxiway U and got a new release with the fuel we had; new to data and departed.

Data retrieved from NASA's ASRS site and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.