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|
Attributes | |
ACN | 172232 |
Time | |
Date | 199103 |
Day | Sun |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | atc facility : mia airport : mco |
State Reference | FL |
Altitude | msl bound lower : 25000 msl bound upper : 25000 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | artcc : zma |
Operator | common carrier : air carrier |
Make Model Name | Large Transport, Low Wing, 3 Turbojet Eng |
Flight Phase | climbout : intermediate altitude cruise other landing other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : second officer |
Qualification | pilot : flight engineer pilot : commercial pilot : atp pilot : instrument |
Experience | flight time last 90 days : 55 flight time total : 4000 flight time type : 55 |
ASRS Report | 172232 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp pilot : commercial pilot : instrument |
Events | |
Anomaly | aircraft equipment problem : less severe |
Independent Detector | other flight crewa |
Resolutory Action | other |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | other |
Narrative:
Shortly after takeoff, F/a (seated on aft jumpseat) reported a scraping noise on takeoff. A level off at an intermediate altitude was initiated and a pilot was sent back to view the aft airstair area. A gap between the airstair and stairwell was observed. After conferring with company maintenance and a dead heading line check captain onboard, crew elected to execute a precautionary landing at mco. Fuel dumping was initiated to get down to landing weight. An uneventful landing followed. Upon lowering aft airstair, a 4-5' strip of wxstripping was missing. Maintenance was completed and flight continued.
Original NASA ASRS Text
Title: AFTER TKOF A FLT ATTENDANT REPORT CAUSED PLT TO VIEW AFT STAIRWELL AREA NOTING A GAP BETWEEN STAIR AND AIRFRAME. FUEL WAS DUMPED AND LNDG AT INTERMEDIATE ARPT MCO WAS MADE FOR MAINTENANCE.
Narrative: SHORTLY AFTER TKOF, F/A (SEATED ON AFT JUMPSEAT) RPTED A SCRAPING NOISE ON TKOF. A LEVEL OFF AT AN INTERMEDIATE ALT WAS INITIATED AND A PLT WAS SENT BACK TO VIEW THE AFT AIRSTAIR AREA. A GAP BTWN THE AIRSTAIR AND STAIRWELL WAS OBSERVED. AFTER CONFERRING WITH COMPANY MAINT AND A DEAD HDG LINE CHK CAPT ONBOARD, CREW ELECTED TO EXECUTE A PRECAUTIONARY LNDG AT MCO. FUEL DUMPING WAS INITIATED TO GET DOWN TO LNDG WEIGHT. AN UNEVENTFUL LNDG FOLLOWED. UPON LOWERING AFT AIRSTAIR, A 4-5' STRIP OF WXSTRIPPING WAS MISSING. MAINT WAS COMPLETED AND FLT CONTINUED.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.