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|
Attributes | |
ACN | 1738223 |
Time | |
Date | 202003 |
Local Time Of Day | 1201-1800 |
Place | |
Locale Reference | ZZZ.Airport |
State Reference | US |
Environment | |
Light | Daylight |
Aircraft 1 | |
Make Model Name | Skyhawk 172/Cutlass 172 |
Operating Under FAR Part | Part 91 |
Flight Phase | Takeoff |
Flight Plan | VFR |
Person 1 | |
Function | Pilot Flying Single Pilot |
Qualification | Flight Crew Private |
Experience | Flight Crew Last 90 Days 2 Flight Crew Total 111 Flight Crew Type 39 |
Events | |
Anomaly | Deviation - Procedural Published Material / Policy Ground Event / Encounter Object |
Narrative:
After my pre-flight inspection; I towed the aircraft out of the hangar; closed the hangar doors and locked them; then I boarded the aircraft; started up; taxied to the run-up area and did my run-up. At this point nothing altered me that anything was wrong. I then taxied to the runway; lined up; announced my departure; then went to full power/throttle when I heard a loud metallic sound and felt a bump. I immediately withdrew the power and announced my aborted takeoff. I taxied back to the ramp; out of the way; and shut down the aircraft. When I got out I realized I had never removed the tow bar from the nose wheel; then I observed the propeller and noticed that both tips had come into contact with the bar and were damaged. I retrieved the damaged tow bar from the runway and pushed the aircraft back to the hangar with the help of some other pilots on the field. Looking back; I simply should have done another walk around of the aircraft (after the pre-flight inspection) before getting into it.
Original NASA ASRS Text
Title: C172 pilot reported an aborted takeoff because the tow bar was still attached.
Narrative: After my pre-flight inspection; I towed the aircraft out of the hangar; closed the hangar doors and locked them; then I boarded the aircraft; started up; taxied to the run-up area and did my run-up. At this point nothing altered me that anything was wrong. I then taxied to the runway; lined up; announced my departure; then went to full power/throttle when I heard a loud metallic sound and felt a bump. I immediately withdrew the power and announced my aborted takeoff. I taxied back to the ramp; out of the way; and shut down the aircraft. When I got out I realized I had never removed the tow bar from the nose wheel; then I observed the propeller and noticed that both tips had come into contact with the bar and were damaged. I retrieved the damaged tow bar from the runway and pushed the aircraft back to the hangar with the help of some other pilots on the field. Looking back; I simply should have done another walk around of the aircraft (after the pre-flight inspection) before getting into it.
Data retrieved from NASA's ASRS site and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.