Narrative:

Approximately 1 hour 40 minutes into flight; during cruise; there was an over voltage indication. While trouble shooting the issue; there was a pop noise and a puff of smoke from the right side under the glare shield. The smoke did not continue on after the initial pop. [Advised ATC]; shed all non essential electric load; pulled the alternator circuit breaker; received vectors toward closest airfield and landed safely. Landing gear; flaps; and boost pump all worked normal with battery power.

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Original NASA ASRS Text

Title: M20 pilot reported diverting due to an alternator failure.

Narrative: Approximately 1 hour 40 minutes into flight; during cruise; there was an over voltage indication. While trouble shooting the issue; there was a pop noise and a puff of smoke from the right side under the glare shield. The smoke did not continue on after the initial pop. [Advised ATC]; shed all non essential electric load; pulled the alternator CB; received vectors toward closest airfield and landed safely. Landing gear; flaps; and boost pump all worked normal with battery power.

Data retrieved from NASA's ASRS site and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.