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|
Attributes | |
ACN | 174993 |
Time | |
Date | 199104 |
Day | Fri |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | airport : owb |
State Reference | KY |
Altitude | agl bound lower : 0 agl bound upper : 0 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Operator | common carrier : air carrier |
Make Model Name | Light Transport, Low Wing, 2 Turboprop Eng |
Flight Phase | climbout : takeoff |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : commercial pilot : instrument |
Experience | flight time last 90 days : 260 flight time total : 2300 |
ASRS Report | 174993 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Events | |
Anomaly | non adherence : published procedure other anomaly |
Independent Detector | other flight crewa |
Resolutory Action | flight crew : overcame equipment problem |
Consequence | Other |
Supplementary | |
Primary Problem | Flight Crew Human Performance |
Air Traffic Incident | Pilot Deviation |
Narrative:
Cleared for takeoff on runway 17 owb. The captain advanced the power levers roughly overlooking the fact that the #2 engine was still on the start lock and the aircraft yawed approximately 45-50 degrees right of centerline. The captain was hesitant to retard the power levers to flight idle allowing the aircraft to do this. I called out twice that the lock was still engaged. After the power levers were retarded the captain called for speeds low and he realigned the aircraft on centerline, asked if takeoff clearance was still good and then proceeded to release the locks on lock engine. Called for speeds high and advanced the power levers for takeoff thrust and departed the area. I do believe this would not have happened if the captain did not advance the power levers so roughly. If they were advanced smoothly, the torque gauges would have showed that the #2 engine was not producing takeoff power.
Original NASA ASRS Text
Title: LTT VEERS OFF CENTERLINE AS POWER IS APPLIED WITH START LOCK STILL ON 1 ENGINE.
Narrative: CLRED FOR TKOF ON RWY 17 OWB. THE CAPT ADVANCED THE PWR LEVERS ROUGHLY OVERLOOKING THE FACT THAT THE #2 ENG WAS STILL ON THE START LOCK AND THE ACFT YAWED APPROX 45-50 DEGS RIGHT OF CENTERLINE. THE CAPT WAS HESITANT TO RETARD THE PWR LEVERS TO FLT IDLE ALLOWING THE ACFT TO DO THIS. I CALLED OUT TWICE THAT THE LOCK WAS STILL ENGAGED. AFTER THE PWR LEVERS WERE RETARDED THE CAPT CALLED FOR SPDS LOW AND HE REALIGNED THE ACFT ON CENTERLINE, ASKED IF TKOF CLRNC WAS STILL GOOD AND THEN PROCEEDED TO RELEASE THE LOCKS ON LOCK ENG. CALLED FOR SPDS HIGH AND ADVANCED THE PWR LEVERS FOR TKOF THRUST AND DEPARTED THE AREA. I DO BELIEVE THIS WOULD NOT HAVE HAPPENED IF THE CAPT DID NOT ADVANCE THE PWR LEVERS SO ROUGHLY. IF THEY WERE ADVANCED SMOOTHLY, THE TORQUE GAUGES WOULD HAVE SHOWED THAT THE #2 ENG WAS NOT PRODUCING TKOF PWR.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.