37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 176224 |
Time | |
Date | 199104 |
Day | Wed |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : dca |
State Reference | DC |
Altitude | agl bound lower : 0 agl bound upper : 0 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Operator | common carrier : air carrier |
Make Model Name | Large Transport, Low Wing, 3 Turbojet Eng |
Flight Phase | ground : preflight |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : second officer |
Qualification | pilot : instrument pilot : commercial pilot : flight engineer |
Experience | flight time last 90 days : 225 flight time total : 6400 flight time type : 820 |
ASRS Report | 176224 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp pilot : instrument pilot : commercial |
Experience | flight time last 90 days : 150 flight time total : 14000 |
ASRS Report | 176033 |
Events | |
Anomaly | non adherence : far non adherence other other anomaly other |
Independent Detector | other flight crewa |
Resolutory Action | other other |
Consequence | Other Other |
Supplementary | |
Primary Problem | Flight Crew Human Performance |
Air Traffic Incident | Pilot Deviation |
Situations | |
Airport | procedure or policy : unspecified |
Narrative:
Crew had normal preflight, flight planning and departure from dca en route to mke. After level off at FL390, I, the second officer, noted that fuel quantity in #1 and #3 main fuel tanks were considerably lower than they should have been. #2 tank was normal. After checking for leaks, etc, we diverted to cle with a normal landing. At cle, the aircraft was checked with no abnormal conditions noted. The aircraft was cleared by maintenance and the flight continued to msp for termination. A possible refueling error was made at dca in that the fuel slip indicated more fuel on board from the previous flight than the aircraft logbook. Also, during the preflight and predep the second officer and the captain 'saw' the correct amount of fuel on the gauges. But the fuel was not apparently in the outboard tanks in correct amounts. Gauges may have been incorrect for some unknown reason. The second officer may have misread the gauges. The captain may have misread the gauges. Corrective action, a positive reconfirmation of the cockpit fuel gauges by the refueler may have helped prevent this problem.
Original NASA ASRS Text
Title: AT CRUISE LEVEL OFF FE REALIZED FUEL GAUGES INDICATED LESS THAN PLANNED FUEL. FLT DIVERTED TO CLE FOR LNDG. REFUELING.
Narrative: CREW HAD NORMAL PREFLT, FLT PLANNING AND DEP FROM DCA ENRTE TO MKE. AFTER LEVEL OFF AT FL390, I, THE S/O, NOTED THAT FUEL QUANTITY IN #1 AND #3 MAIN FUEL TANKS WERE CONSIDERABLY LOWER THAN THEY SHOULD HAVE BEEN. #2 TANK WAS NORMAL. AFTER CHKING FOR LEAKS, ETC, WE DIVERTED TO CLE WITH A NORMAL LNDG. AT CLE, THE ACFT WAS CHKED WITH NO ABNORMAL CONDITIONS NOTED. THE ACFT WAS CLRED BY MAINT AND THE FLT CONTINUED TO MSP FOR TERMINATION. A POSSIBLE REFUELING ERROR WAS MADE AT DCA IN THAT THE FUEL SLIP INDICATED MORE FUEL ON BOARD FROM THE PREVIOUS FLT THAN THE ACFT LOGBOOK. ALSO, DURING THE PREFLT AND PREDEP THE S/O AND THE CAPT 'SAW' THE CORRECT AMOUNT OF FUEL ON THE GAUGES. BUT THE FUEL WAS NOT APPARENTLY IN THE OUTBOARD TANKS IN CORRECT AMOUNTS. GAUGES MAY HAVE BEEN INCORRECT FOR SOME UNKNOWN REASON. THE S/O MAY HAVE MISREAD THE GAUGES. THE CAPT MAY HAVE MISREAD THE GAUGES. CORRECTIVE ACTION, A POSITIVE RECONFIRMATION OF THE COCKPIT FUEL GAUGES BY THE REFUELER MAY HAVE HELPED PREVENT THIS PROB.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.