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|
Attributes | |
ACN | 188632 |
Time | |
Date | 199109 |
Day | Tue |
Local Time Of Day | 1801 To 2400 |
Place | |
Locale Reference | airport : sdf |
State Reference | KY |
Altitude | msl bound lower : 1300 msl bound upper : 1300 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Operator | general aviation : instructional |
Make Model Name | Helicopter |
Flight Phase | climbout : intermediate altitude cruise other |
Flight Plan | None |
Person 1 | |
Affiliation | Other |
Function | flight crew : single pilot |
Qualification | pilot : commercial pilot : instrument |
Experience | flight time last 90 days : 58 flight time total : 7500 flight time type : 352 |
ASRS Report | 188632 |
Events | |
Anomaly | aircraft equipment problem : critical non adherence : far other anomaly other |
Independent Detector | other flight crewa |
Resolutory Action | flight crew : declared emergency none taken : detected after the fact |
Consequence | other |
Supplementary | |
Primary Problem | Flight Crew Human Performance |
Air Traffic Incident | Pilot Deviation |
Narrative:
During preflight, I removed the right engine cowling in order to loosen the engine ejector duct (exhaust) clamp as it was in contact with the #2 and 3 bearing oil pressure line, and rotated the clamp a few degrees. (I hold an a and P certificate also). I replaced the cowling and latched the top dzus fasteners but failed to latch the lower fasteners. After takeoff, climb out and the start of cruise flight, the right engine cowling came off the aircraft, striking the bottom of the 4 main rotor blades, then fell into the ohio river. I proceeded to make an uneventful precautionary landing in a field next to the river. Other than a slight vibration when the cowling departed the aircraft, there was no adverse control problems what so ever. I readily admit that this incident occurred because I failed to complete an adequate preflight.
Original NASA ASRS Text
Title: FBO HELI LOST AN ENG COWL AFTER TKOF AND HAD TO MAKE AN OFF ARPT LNDG.
Narrative: DURING PREFLT, I REMOVED THE R ENG COWLING IN ORDER TO LOOSEN THE ENG EJECTOR DUCT (EXHAUST) CLAMP AS IT WAS IN CONTACT WITH THE #2 AND 3 BEARING OIL PRESSURE LINE, AND ROTATED THE CLAMP A FEW DEGS. (I HOLD AN A AND P CERTIFICATE ALSO). I REPLACED THE COWLING AND LATCHED THE TOP DZUS FASTENERS BUT FAILED TO LATCH THE LOWER FASTENERS. AFTER TKOF, CLB OUT AND THE START OF CRUISE FLT, THE R ENG COWLING CAME OFF THE ACFT, STRIKING THE BOTTOM OF THE 4 MAIN ROTOR BLADES, THEN FELL INTO THE OHIO RIVER. I PROCEEDED TO MAKE AN UNEVENTFUL PRECAUTIONARY LNDG IN A FIELD NEXT TO THE RIVER. OTHER THAN A SLIGHT VIBRATION WHEN THE COWLING DEPARTED THE ACFT, THERE WAS NO ADVERSE CTL PROBLEMS WHAT SO EVER. I READILY ADMIT THAT THIS INCIDENT OCCURRED BECAUSE I FAILED TO COMPLETE AN ADEQUATE PREFLT.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.