37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 191640 |
Time | |
Date | 199110 |
Day | Sat |
Local Time Of Day | 1801 To 2400 |
Place | |
Locale Reference | airport : cvg |
State Reference | OH |
Altitude | msl bound lower : 9000 msl bound upper : 9000 |
Environment | |
Flight Conditions | Mixed |
Light | Dusk |
Aircraft 1 | |
Controlling Facilities | tracon : ord |
Operator | common carrier : air carrier |
Make Model Name | Light Transport, Low Wing, 2 Turboprop Eng |
Navigation In Use | Other Other |
Flight Phase | climbout : intermediate altitude |
Route In Use | enroute airway : cvg |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Experience | flight time last 90 days : 180 flight time total : 6000 flight time type : 3500 |
ASRS Report | 191640 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : commercial pilot : instrument |
Events | |
Anomaly | aircraft equipment problem : critical |
Independent Detector | aircraft equipment other aircraft equipment : unspecified other flight crewa |
Resolutory Action | flight crew : declared emergency none taken : unable other |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | other |
Narrative:
10 mins after takeoff from kcvg, the right dc generator failed as evidenced by the right generator light and cwp light coming on. Bus tie connect light also came on indicating transfer of right generator load to left generator. In accordance with flight man procedure, 2 attempts were made to reset generator and results were negative. Flight diverted back to kcvg and landed without further incident. Aircraft repaired after landing.
Original NASA ASRS Text
Title: COMMUTER ACFT HAS GENERATOR PROBLEM AFTER DEP. RETURN LAND.
Narrative: 10 MINS AFTER TKOF FROM KCVG, THE R DC GENERATOR FAILED AS EVIDENCED BY THE R GENERATOR LIGHT AND CWP LIGHT COMING ON. BUS TIE CONNECT LIGHT ALSO CAME ON INDICATING TRANSFER OF R GENERATOR LOAD TO L GENERATOR. IAW FLT MAN PROC, 2 ATTEMPTS WERE MADE TO RESET GENERATOR AND RESULTS WERE NEGATIVE. FLT DIVERTED BACK TO KCVG AND LANDED WITHOUT FURTHER INCIDENT. ACFT REPAIRED AFTER LNDG.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.