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|
Attributes | |
ACN | 192202 |
Time | |
Date | 199110 |
Day | Mon |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | airport : den |
State Reference | CO |
Altitude | agl bound lower : 0 agl bound upper : 0 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Operator | common carrier : air carrier |
Make Model Name | Medium Transport, High Wing, 2 Turboprop Eng |
Flight Phase | climbout : takeoff other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : cfi pilot : instrument pilot : commercial pilot : atp |
Experience | flight time last 90 days : 270 flight time total : 7000 flight time type : 1500 |
ASRS Report | 192202 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : commercial pilot : instrument |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | aircraft equipment other aircraft equipment : unspecified other flight crewa |
Resolutory Action | flight crew : declared emergency flight crew : overcame equipment problem |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | other |
Narrative:
As power was added for takeoff and takeoff roll began, right propeller was slow to accelerate. At approximately 10 KTS ground speed, and with left propeller indicating 98 percent, right propeller was indicating 78 percent, ccas engine and electric warnings were activated with low pitch and acw caution lights. Torque on right engine indicating 17.1 percent with power lever beyond 60 percent. Takeoff aborted. After clearing runway, acw generator reset per aom. Static runup normal. CTAF notified of acw generator trip. Coordinated with iah maintenance center who concurred that we could continue. Subsequent takeoff normal.
Original NASA ASRS Text
Title: COMMUTER MDT HAD TO ABORT A TKOF FROM DEN BECAUSE OF SLOW PWR ACCELERATION ON 1 ENG.
Narrative: AS PWR WAS ADDED FOR TKOF AND TKOF ROLL BEGAN, R PROP WAS SLOW TO ACCELERATE. AT APPROX 10 KTS GND SPD, AND WITH L PROP INDICATING 98 PERCENT, R PROP WAS INDICATING 78 PERCENT, CCAS ENG AND ELECTRIC WARNINGS WERE ACTIVATED WITH LOW PITCH AND ACW CAUTION LIGHTS. TORQUE ON R ENG INDICATING 17.1 PERCENT WITH PWR LEVER BEYOND 60 PERCENT. TKOF ABORTED. AFTER CLRING RWY, ACW GENERATOR RESET PER AOM. STATIC RUNUP NORMAL. CTAF NOTIFIED OF ACW GENERATOR TRIP. COORDINATED WITH IAH MAINT CENTER WHO CONCURRED THAT WE COULD CONTINUE. SUBSEQUENT TKOF NORMAL.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.