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|
Attributes | |
ACN | 195104 |
Time | |
Date | 199111 |
Day | Wed |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | airport : ord |
State Reference | IL |
Altitude | msl bound lower : 7000 msl bound upper : 7000 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tracon : ord artcc : zdc |
Operator | common carrier : air carrier |
Make Model Name | Medium Transport |
Navigation In Use | Other Other |
Flight Phase | descent : approach descent other |
Flight Plan | IFR |
Aircraft 2 | |
Operator | common carrier : air carrier |
Make Model Name | Large Transport, Low Wing, 3 Turbojet Eng |
Flight Phase | descent : approach |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Experience | flight time last 90 days : 200 flight time total : 10000 |
ASRS Report | 195104 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : commercial pilot : atp pilot : instrument |
Events | |
Anomaly | other anomaly other |
Independent Detector | other flight crewa |
Resolutory Action | flight crew : regained aircraft control |
Consequence | Other |
Supplementary | |
Air Traffic Incident | other |
Narrative:
After deere intersection cleared ord VOR at 7000 encountered wake from preceding large transport at same altitude approximately visually appeared to be the required 3 mi separation by ATC. Aircraft started roll to the left and started buffeting. Autoplt, yaw damper and adu failed, negative G's were felt and cockpit and cabin items were dislodged and a very rough shaking was experienced. Flight attendant was hurt, minor injuries. Aircraft was inspected for damage. The only damage I'm aware of was inside the aircraft from the flight attendant being tossed around and bent curtain rod. The conditions of flight were smooth air and the legal separation does not appear to be adequate under some atmospheric conditions such as smooth air. At this point in time I understand this is classified as an incident and the NTSB is investigating it.
Original NASA ASRS Text
Title: MDT ENCOUNTERS WAKE TURB EVEN THOUGH PROPER 3 MI SPACING EXISTED.
Narrative: AFTER DEERE INTXN CLRED ORD VOR AT 7000 ENCOUNTERED WAKE FROM PRECEDING LGT AT SAME ALT APPROX VISUALLY APPEARED TO BE THE REQUIRED 3 MI SEPARATION BY ATC. ACFT STARTED ROLL TO THE L AND STARTED BUFFETING. AUTOPLT, YAW DAMPER AND ADU FAILED, NEGATIVE G'S WERE FELT AND COCKPIT AND CABIN ITEMS WERE DISLODGED AND A VERY ROUGH SHAKING WAS EXPERIENCED. FLT ATTENDANT WAS HURT, MINOR INJURIES. ACFT WAS INSPECTED FOR DAMAGE. THE ONLY DAMAGE I'M AWARE OF WAS INSIDE THE ACFT FROM THE FLT ATTENDANT BEING TOSSED AROUND AND BENT CURTAIN ROD. THE CONDITIONS OF FLT WERE SMOOTH AIR AND THE LEGAL SEPARATION DOES NOT APPEAR TO BE ADEQUATE UNDER SOME ATMOSPHERIC CONDITIONS SUCH AS SMOOTH AIR. AT THIS POINT IN TIME I UNDERSTAND THIS IS CLASSIFIED AS AN INCIDENT AND THE NTSB IS INVESTIGATING IT.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.