37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 209661 |
Time | |
Date | 199205 |
Day | Fri |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | atc facility : dtw |
State Reference | MI |
Altitude | msl bound lower : 13000 msl bound upper : 23000 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | artcc : zau |
Operator | common carrier : air carrier |
Make Model Name | Widebody, Low Wing, 3 Turbojet Eng |
Navigation In Use | Other |
Flight Phase | climbout : intermediate altitude other |
Route In Use | enroute : direct enroute airway : zau |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : second officer |
Qualification | pilot : commercial pilot : flight engineer pilot : instrument pilot : atp |
Experience | flight time last 90 days : 250 flight time total : 3000 flight time type : 600 |
ASRS Report | 209661 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Events | |
Anomaly | aircraft equipment problem : less severe other anomaly other |
Independent Detector | other other : unspecified |
Resolutory Action | flight crew : declared emergency none taken : unable other |
Consequence | other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | other |
Narrative:
While climbing through 13000 ft to FL230, the senior flight attendant came to the cockpit and stated that the other flight attendants in the rear of the cabin smelled an electrical odor from the area of the 3L and 3R doors to the aft of the cabin. No smoke was visible. I went aft and checked the area and found a strong electrical burning odor, but no smoke. While checking the ceiling and lavatory area, the smoke alarms in the aft lavatories went off. Again, no smoke was visible. Both flight attendants in the rear grabbed fire bottles and prepared to combat a fire. No fire broke out and no smoke was visible. I assigned the flight attendants in the rear to watch the lavatory area and keep us informed if fire or smoke did become apparent. I advised the lead flight attendant to secure the cabin and prepare for return and landing at dtw. After informing the captain of the situation, we decided to continue back to dtw since no smoke or fire was present. Kalamazoo would have been our option if the situation had turned bad. The smoke removal checklist was not necessary, although it was reviewed silently. We asked ATC and were cleared to exceed 250 KTS below 10000 ft. An emergency was declared. An uneventful and overweight landing was made at dtw. No evacuate/evacuation was made. The fire department came on board and investigated, and no evidence of a fire was found. We swapped airplanes and an uneventful trip to las was completed. Maintenance found that a decoder for the multiplex system in the cabin overhead had shorted out resulting in the burning of some electrical wiring. A fire could have resulted if quick action had not been taken. I also feel the crew worked and performed very well together as a result of the recent cockpit resource management class at our carrier.
Original NASA ASRS Text
Title: ACFT EQUIP PROBLEM DETECTED BY SMELL OF SMOKE. ACFT RETURN LANDS AFTER EMER DECLARED.
Narrative: WHILE CLBING THROUGH 13000 FT TO FL230, THE SENIOR FLT ATTENDANT CAME TO THE COCKPIT AND STATED THAT THE OTHER FLT ATTENDANTS IN THE REAR OF THE CABIN SMELLED AN ELECTRICAL ODOR FROM THE AREA OF THE 3L AND 3R DOORS TO THE AFT OF THE CABIN. NO SMOKE WAS VISIBLE. I WENT AFT AND CHKED THE AREA AND FOUND A STRONG ELECTRICAL BURNING ODOR, BUT NO SMOKE. WHILE CHKING THE CEILING AND LAVATORY AREA, THE SMOKE ALARMS IN THE AFT LAVATORIES WENT OFF. AGAIN, NO SMOKE WAS VISIBLE. BOTH FLT ATTENDANTS IN THE REAR GRABBED FIRE BOTTLES AND PREPARED TO COMBAT A FIRE. NO FIRE BROKE OUT AND NO SMOKE WAS VISIBLE. I ASSIGNED THE FLT ATTENDANTS IN THE REAR TO WATCH THE LAVATORY AREA AND KEEP US INFORMED IF FIRE OR SMOKE DID BECOME APPARENT. I ADVISED THE LEAD FLT ATTENDANT TO SECURE THE CABIN AND PREPARE FOR RETURN AND LNDG AT DTW. AFTER INFORMING THE CAPT OF THE SITUATION, WE DECIDED TO CONTINUE BACK TO DTW SINCE NO SMOKE OR FIRE WAS PRESENT. KALAMAZOO WOULD HAVE BEEN OUR OPTION IF THE SITUATION HAD TURNED BAD. THE SMOKE REMOVAL CHKLIST WAS NOT NECESSARY, ALTHOUGH IT WAS REVIEWED SILENTLY. WE ASKED ATC AND WERE CLRED TO EXCEED 250 KTS BELOW 10000 FT. AN EMER WAS DECLARED. AN UNEVENTFUL AND OVERWT LNDG WAS MADE AT DTW. NO EVAC WAS MADE. THE FIRE DEPT CAME ON BOARD AND INVESTIGATED, AND NO EVIDENCE OF A FIRE WAS FOUND. WE SWAPPED AIRPLANES AND AN UNEVENTFUL TRIP TO LAS WAS COMPLETED. MAINT FOUND THAT A DECODER FOR THE MULTIPLEX SYS IN THE CABIN OVERHEAD HAD SHORTED OUT RESULTING IN THE BURNING OF SOME ELECTRICAL WIRING. A FIRE COULD HAVE RESULTED IF QUICK ACTION HAD NOT BEEN TAKEN. I ALSO FEEL THE CREW WORKED AND PERFORMED VERY WELL TOGETHER AS A RESULT OF THE RECENT COCKPIT RESOURCE MGMNT CLASS AT OUR CARRIER.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.