37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 209725 |
Time | |
Date | 199205 |
Day | Sat |
Local Time Of Day | 1801 To 2400 |
Place | |
Locale Reference | airport : cvg |
State Reference | OH |
Altitude | msl bound lower : 1600 msl bound upper : 1600 |
Environment | |
Flight Conditions | Marginal |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tracon : cvg |
Operator | common carrier : air carrier |
Make Model Name | Medium Large Transport, Low Wing, 2 Turbojet Eng |
Flight Phase | climbout : takeoff landing : missed approach landing other |
Route In Use | enroute : on vectors |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : instrument pilot : flight engineer pilot : commercial pilot : atp pilot : cfi |
Experience | flight time last 90 days : 200 flight time total : 10500 flight time type : 500 |
ASRS Report | 209725 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : atp |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | aircraft equipment other aircraft equipment : unspecified |
Resolutory Action | flight crew : declared emergency other |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Narrative:
On takeoff cvg at 1600 MSL (approximately 800 AGL), right engine fire warning came on. Fire warning did not go out until fire handle was pulled. Did fire test and was good. Suspected pneumatic leak. Elected not to fire fire bottles. Flight attendant checked engine for damage and smoke. Notified ATC and cleaned up and climbed on 1 engine to go back for approach. During approach, RVR dropped below mins (2400) for single engine approach. Did go around from approximately 2200 MSL/1300 AGL. Returned for second approach. RVR 6000 plus and landed uneventfully. Maintenance found leaking eighth stage duct and blown thirteenth stage duct going to anti-ice valve. From takeoff to landing was approximately 30 mins even though we never got more than 15 mi from airport due to WX and doing 2 approachs. Factors were thunderstorm and rainshowers in area, heavy airplane, gusty wind, flight was very busy for awhile because of 2 man crew. Would have been nice to have a third crew member. Old airplane (approximately 1968). If we did not elect to do go around early, it would have been difficult if not impossible once gear and flaps were down. Training helped. Just like in simulator.
Original NASA ASRS Text
Title: ACR HAS FIRE WARNING AFTER LIFT OFF. RETURN BUT RVR BELOW SINGLE ENG MINS. GAR AND SECOND APCH RVR OK.
Narrative: ON TKOF CVG AT 1600 MSL (APPROX 800 AGL), R ENG FIRE WARNING CAME ON. FIRE WARNING DID NOT GO OUT UNTIL FIRE HANDLE WAS PULLED. DID FIRE TEST AND WAS GOOD. SUSPECTED PNEUMATIC LEAK. ELECTED NOT TO FIRE FIRE BOTTLES. FLT ATTENDANT CHKED ENG FOR DAMAGE AND SMOKE. NOTIFIED ATC AND CLEANED UP AND CLBED ON 1 ENG TO GO BACK FOR APCH. DURING APCH, RVR DROPPED BELOW MINS (2400) FOR SINGLE ENG APCH. DID GAR FROM APPROX 2200 MSL/1300 AGL. RETURNED FOR SECOND APCH. RVR 6000 PLUS AND LANDED UNEVENTFULLY. MAINT FOUND LEAKING EIGHTH STAGE DUCT AND BLOWN THIRTEENTH STAGE DUCT GOING TO ANTI-ICE VALVE. FROM TKOF TO LNDG WAS APPROX 30 MINS EVEN THOUGH WE NEVER GOT MORE THAN 15 MI FROM ARPT DUE TO WX AND DOING 2 APCHS. FACTORS WERE TSTM AND RAINSHOWERS IN AREA, HVY AIRPLANE, GUSTY WIND, FLT WAS VERY BUSY FOR AWHILE BECAUSE OF 2 MAN CREW. WOULD HAVE BEEN NICE TO HAVE A THIRD CREW MEMBER. OLD AIRPLANE (APPROX 1968). IF WE DID NOT ELECT TO DO GAR EARLY, IT WOULD HAVE BEEN DIFFICULT IF NOT IMPOSSIBLE ONCE GEAR AND FLAPS WERE DOWN. TRAINING HELPED. JUST LIKE IN SIMULATOR.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.