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|
Attributes | |
ACN | 222695 |
Time | |
Date | 199210 |
Day | Sat |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : mia |
State Reference | FL |
Altitude | agl bound lower : 0 agl bound upper : 1700 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tracon : mia |
Operator | general aviation : instructional |
Make Model Name | Small Aircraft, High Wing, 1 Eng, Fixed Gear |
Flight Phase | descent : approach landing other other |
Route In Use | enroute : on vectors |
Flight Plan | IFR |
Person 1 | |
Affiliation | Other |
Function | flight crew : single pilot |
Qualification | pilot : instrument pilot : commercial |
Experience | flight time last 90 days : 25 flight time total : 203 |
ASRS Report | 222695 |
Person 2 | |
Affiliation | government : faa |
Function | controller : approach |
Qualification | controller : radar |
Events | |
Anomaly | aircraft equipment problem : critical non adherence : far other anomaly other |
Independent Detector | other flight crewa |
Resolutory Action | flight crew : declared emergency other |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | Pilot Deviation |
Narrative:
The aircraft ran out of gas approximately 5 mi northwest of destination, while being vectored for ILS final approach. When cleared to initial approach altitude, the engine quit. The fuel gauges were reading 1/4 full (both) which corresponding to our calculations of 1 plus 08 hours of fuel remaining. The only place to land was a private road inside of gravel pit. We informed miami approach of our situation and proceeded with an emergency landing without power. My copilot and I are both commercial instructor pilots and we both kept very accurate flight logs. We both checked our fuel supply prior to takeoff and the tanks were completely full. We believe that the left fuel tank had an undetected leak and the corresponding gauge was inaccurate. We did not notice the leak on preflight since it was raining. Also we believe that the engine was not burning the published fuel flow. Although the engine was leaned according to operations handbook with the egt the engine might have been burning richer than indicative in poh. The aircraft and the occupants were both unharmed.
Original NASA ASRS Text
Title: EMER FORCED OFF ARPT LNDG MADE AFTER SMA EXPERIENCES FUEL EXHAUSTION.
Narrative: THE ACFT RAN OUT OF GAS APPROX 5 MI NW OF DEST, WHILE BEING VECTORED FOR ILS FINAL APCH. WHEN CLRED TO INITIAL APCH ALT, THE ENG QUIT. THE FUEL GAUGES WERE READING 1/4 FULL (BOTH) WHICH CORRESPONDING TO OUR CALCULATIONS OF 1 PLUS 08 HRS OF FUEL REMAINING. THE ONLY PLACE TO LAND WAS A PRIVATE ROAD INSIDE OF GRAVEL PIT. WE INFORMED MIAMI APCH OF OUR SITUATION AND PROCEEDED WITH AN EMER LNDG WITHOUT PWR. MY COPLT AND I ARE BOTH COMMERCIAL INSTRUCTOR PLTS AND WE BOTH KEPT VERY ACCURATE FLT LOGS. WE BOTH CHKED OUR FUEL SUPPLY PRIOR TO TKOF AND THE TANKS WERE COMPLETELY FULL. WE BELIEVE THAT THE L FUEL TANK HAD AN UNDETECTED LEAK AND THE CORRESPONDING GAUGE WAS INACCURATE. WE DID NOT NOTICE THE LEAK ON PREFLT SINCE IT WAS RAINING. ALSO WE BELIEVE THAT THE ENG WAS NOT BURNING THE PUBLISHED FUEL FLOW. ALTHOUGH THE ENG WAS LEANED ACCORDING TO OPS HANDBOOK WITH THE EGT THE ENG MIGHT HAVE BEEN BURNING RICHER THAN INDICATIVE IN POH. THE ACFT AND THE OCCUPANTS WERE BOTH UNHARMED.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.