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|
Attributes | |
ACN | 225156 |
Time | |
Date | 199210 |
Day | Wed |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : tus |
State Reference | AZ |
Altitude | agl bound lower : 0 agl bound upper : 0 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Operator | general aviation : corporate |
Make Model Name | Small Transport, Low Wing, 2 Turboprop Eng |
Flight Phase | ground : preflight |
Flight Plan | IFR |
Person 1 | |
Affiliation | Other |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp pilot : instrument pilot : commercial pilot : cfi |
Experience | flight time last 90 days : 50 flight time total : 7100 flight time type : 4600 |
ASRS Report | 225156 |
Person 2 | |
Affiliation | Other |
Function | flight crew : first officer |
Qualification | pilot : atp |
Experience | flight time last 90 days : 35 flight time total : 17500 flight time type : 75 |
ASRS Report | 225150 |
Events | |
Anomaly | aircraft equipment problem : critical non adherence : far |
Independent Detector | other other : unspecified |
Resolutory Action | none taken : detected after the fact |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | Pilot Deviation |
Narrative:
We had landed at tus after experiencing a gear problem in which we had to manually pump down the landing gear. After landing, we contacted maintenance, described our problem and their recommendation was to fly home with the gear down and locked. We decided it was reasonably safe to do so and we boarded 2 passenger and took off for san. After arriving safely in san, we again discussed the situation and came to some different conclusions on the validity of our judgement. The first was we had no guaranteed performance for the climb should we have lost an engine on takeoff. (Though the aircraft was 'light'). Second was that it was illegal to accomplish without a ferry permit since this condition was not addressed in our MEL. After discussing this again with the other pilot, we agreed that we had made a poor judgement and would not be pressured to have this occur again (ever!). Supplemental information from acn 225150. In past 12 months gear circuit breaker had tripped causing crew to manually crank down gear at least on 2 occasions. Intensive involvement with maintenance department, factory, and others could not find problem.
Original NASA ASRS Text
Title: AN CPR SMT FLEW A TRIP WITH PAX WITH THE LNDG GEAR DOWN IN VIOLATION OF THE MEL AND WITH NO FERRY PERMIT.
Narrative: WE HAD LANDED AT TUS AFTER EXPERIENCING A GEAR PROBLEM IN WHICH WE HAD TO MANUALLY PUMP DOWN THE LNDG GEAR. AFTER LNDG, WE CONTACTED MAINT, DESCRIBED OUR PROBLEM AND THEIR RECOMMENDATION WAS TO FLY HOME WITH THE GEAR DOWN AND LOCKED. WE DECIDED IT WAS REASONABLY SAFE TO DO SO AND WE BOARDED 2 PAX AND TOOK OFF FOR SAN. AFTER ARRIVING SAFELY IN SAN, WE AGAIN DISCUSSED THE SITUATION AND CAME TO SOME DIFFERENT CONCLUSIONS ON THE VALIDITY OF OUR JUDGEMENT. THE FIRST WAS WE HAD NO GUARANTEED PERFORMANCE FOR THE CLB SHOULD WE HAVE LOST AN ENG ON TKOF. (THOUGH THE ACFT WAS 'LIGHT'). SECOND WAS THAT IT WAS ILLEGAL TO ACCOMPLISH WITHOUT A FERRY PERMIT SINCE THIS CONDITION WAS NOT ADDRESSED IN OUR MEL. AFTER DISCUSSING THIS AGAIN WITH THE OTHER PLT, WE AGREED THAT WE HAD MADE A POOR JUDGEMENT AND WOULD NOT BE PRESSURED TO HAVE THIS OCCUR AGAIN (EVER!). SUPPLEMENTAL INFO FROM ACN 225150. IN PAST 12 MONTHS GEAR CIRCUIT BREAKER HAD TRIPPED CAUSING CREW TO MANUALLY CRANK DOWN GEAR AT LEAST ON 2 OCCASIONS. INTENSIVE INVOLVEMENT WITH MAINT DEPT, FACTORY, AND OTHERS COULD NOT FIND PROBLEM.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.