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|
Attributes | |
ACN | 235299 |
Time | |
Date | 199302 |
Day | Sat |
Local Time Of Day | 1801 To 2400 |
Place | |
Locale Reference | airport : rsw |
State Reference | FL |
Altitude | agl bound lower : 0 agl bound upper : 0 |
Environment | |
Flight Conditions | VMC |
Light | Dusk |
Aircraft 1 | |
Operator | common carrier : air carrier |
Make Model Name | Medium Large Transport, Low Wing, 2 Turbojet Eng |
Navigation In Use | Other Other |
Flight Phase | climbout : takeoff |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : instrument pilot : flight engineer pilot : commercial pilot : atp |
Experience | flight time last 90 days : 180 flight time total : 12000 flight time type : 3000 |
ASRS Report | 235299 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : flight engineer pilot : cfi pilot : atp |
Experience | flight time last 90 days : 140 flight time total : 14000 flight time type : 2000 |
ASRS Report | 235151 |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | aircraft equipment other aircraft equipment : unspecified |
Resolutory Action | flight crew : rejected takeoff |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | other |
Narrative:
The first officer was making the takeoff. At approximately 90 KTS we heard a very loud bang followed almost immediately by a burning smell in the cockpit. I took control of the aircraft and aborted the takeoff. I taxied clear of the runway. We notified tower and accomplished our checklists. The air (smell) in the cabin cleared almost immediately, engine indications were normal, and since the aircraft seemed ok we returned to the gate. Subsequent inspection revealed blood on the #1 engine intake and feathers on the first stage compressor blades. Some blades also appeared to be bent. I notified the company dispatcher and flight operations duty officer. There no injuries or medical problems with any passenger.
Original NASA ASRS Text
Title: FLC OF ACR MLG ACFT ABORTED TKOF AFTER LOUD BANG AND SMOKE SMELL DUE TO A BIRD STRIKE.
Narrative: THE FO WAS MAKING THE TKOF. AT APPROX 90 KTS WE HEARD A VERY LOUD BANG FOLLOWED ALMOST IMMEDIATELY BY A BURNING SMELL IN THE COCKPIT. I TOOK CTL OF THE ACFT AND ABORTED THE TKOF. I TAXIED CLR OF THE RWY. WE NOTIFIED TWR AND ACCOMPLISHED OUR CHKLISTS. THE AIR (SMELL) IN THE CABIN CLRED ALMOST IMMEDIATELY, ENG INDICATIONS WERE NORMAL, AND SINCE THE ACFT SEEMED OK WE RETURNED TO THE GATE. SUBSEQUENT INSPECTION REVEALED BLOOD ON THE #1 ENG INTAKE AND FEATHERS ON THE FIRST STAGE COMPRESSOR BLADES. SOME BLADES ALSO APPEARED TO BE BENT. I NOTIFIED THE COMPANY DISPATCHER AND FLT OPS DUTY OFFICER. THERE NO INJURIES OR MEDICAL PROBS WITH ANY PAX.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.