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|
Attributes | |
ACN | 237516 |
Time | |
Date | 199303 |
Day | Fri |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | airport : mdt |
State Reference | PA |
Altitude | agl bound lower : 0 agl bound upper : 0 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tower : gfk |
Operator | common carrier : air carrier |
Make Model Name | Medium Transport, High Wing, 2 Turboprop Eng |
Flight Phase | climbout : takeoff other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Experience | flight time last 90 days : 150 flight time total : 11000 flight time type : 2200 |
ASRS Report | 237516 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : instrument pilot : commercial |
Events | |
Anomaly | aircraft equipment problem : critical non adherence : published procedure other anomaly other |
Independent Detector | other flight crewa |
Resolutory Action | flight crew : rejected takeoff |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | Pilot Deviation |
Narrative:
While executing the takeoff roll I noticed the control yoke had a left banking pressure. I then glanced down at the trim and noticed the trim indicator indicated full left trim. The decision was made to abort the takeoff. After taxiing clear of the runway, the trim returned to neutral and appeared to be operating fine. The aircraft was taxied back to the runway 31 runup pad and maintenance was radioed and notified of the occurrence. I told maintenance that the trim was reset and the out of trim situation seemed resolved. After clearing up an additional maintenance problem the takeoff and flight was completed without further complications.
Original NASA ASRS Text
Title: TKOF ABORTED DUE TO AILERON TRIM BEING DISPLACED FULLY L.
Narrative: WHILE EXECUTING THE TKOF ROLL I NOTICED THE CTL YOKE HAD A L BANKING PRESSURE. I THEN GLANCED DOWN AT THE TRIM AND NOTICED THE TRIM INDICATOR INDICATED FULL L TRIM. THE DECISION WAS MADE TO ABORT THE TKOF. AFTER TAXIING CLR OF THE RWY, THE TRIM RETURNED TO NEUTRAL AND APPEARED TO BE OPERATING FINE. THE ACFT WAS TAXIED BACK TO THE RWY 31 RUNUP PAD AND MAINT WAS RADIOED AND NOTIFIED OF THE OCCURRENCE. I TOLD MAINT THAT THE TRIM WAS RESET AND THE OUT OF TRIM SIT SEEMED RESOLVED. AFTER CLRING UP AN ADDITIONAL MAINT PROB THE TKOF AND FLT WAS COMPLETED WITHOUT FURTHER COMPLICATIONS.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.