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|
Attributes | |
ACN | 254021 |
Time | |
Date | 199310 |
Day | Fri |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | airport : tiw |
State Reference | WA |
Altitude | agl bound lower : 0 agl bound upper : 2300 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Operator | general aviation : instructional |
Make Model Name | Small Aircraft, High Wing, 1 Eng, Fixed Gear |
Flight Phase | cruise other landing other other |
Flight Plan | None |
Person 1 | |
Affiliation | Other |
Function | instruction : trainee |
Qualification | pilot : private |
Experience | flight time last 90 days : 20 flight time total : 82 flight time type : 3 |
ASRS Report | 254021 |
Person 2 | |
Affiliation | Other |
Function | instruction : instructor |
Qualification | pilot : cfi pilot : commercial pilot : instrument |
Experience | flight time last 90 days : 200 flight time total : 1540 flight time type : 400 |
ASRS Report | 253921 |
Events | |
Anomaly | aircraft equipment problem : critical conflict : ground critical other anomaly other other spatial deviation |
Independent Detector | other flight crewa |
Resolutory Action | flight crew : declared emergency none taken : unable |
Consequence | faa : investigated other |
Supplementary | |
Primary Problem | Aircraft |
Narrative:
Loss of engine power occurred during a training maneuver. Partial power was restored, but not enough to maintain flight. We landed the airplane in a pasture. No injuries. Callback conversation with reporter revealed the following information: the reporting trainee pilot states that the aircraft landed on its main gear. The nose gear came down hard. The nose gear broke off. The spinner dug in, and the aircraft flipped onto its back. The aircraft was probably 'totaled' by the insurance company. The reporter has sent a report to the NTSB, but has not since heard from the FAA or the NTSB (10 weeks have passed). The reporter states that the carburetor heat box was destroyed in the incident, but he believes that the incident was caused by carburetor ice. The engine was run briefly after the incident. The reporter states that he believes that the high skill level of the instructor saved lives. Supplemental information from acn 253921: the student performed all required checks, fuel, mixture, throttle, carburetor heat, ignition, master, and primer. All were in proper place. The throttle was closed. Around 1000 MSL to 1200 MSL, I instructed student to execute a go around. There was no power.
Original NASA ASRS Text
Title: AN SMA MADE AN OFF ARPT LNDG AFTER AN ENG FAILURE.
Narrative: LOSS OF ENG PWR OCCURRED DURING A TRAINING MANEUVER. PARTIAL PWR WAS RESTORED, BUT NOT ENOUGH TO MAINTAIN FLT. WE LANDED THE AIRPLANE IN A PASTURE. NO INJURIES. CALLBACK CONVERSATION WITH RPTR REVEALED THE FOLLOWING INFO: THE RPTING TRAINEE PLT STATES THAT THE ACFT LANDED ON ITS MAIN GEAR. THE NOSE GEAR CAME DOWN HARD. THE NOSE GEAR BROKE OFF. THE SPINNER DUG IN, AND THE ACFT FLIPPED ONTO ITS BACK. THE ACFT WAS PROBABLY 'TOTALED' BY THE INSURANCE COMPANY. THE RPTR HAS SENT A RPT TO THE NTSB, BUT HAS NOT SINCE HEARD FROM THE FAA OR THE NTSB (10 WKS HAVE PASSED). THE RPTR STATES THAT THE CARB HEAT BOX WAS DESTROYED IN THE INCIDENT, BUT HE BELIEVES THAT THE INCIDENT WAS CAUSED BY CARB ICE. THE ENG WAS RUN BRIEFLY AFTER THE INCIDENT. THE RPTR STATES THAT HE BELIEVES THAT THE HIGH SKILL LEVEL OF THE INSTRUCTOR SAVED LIVES. SUPPLEMENTAL INFO FROM ACN 253921: THE STUDENT PERFORMED ALL REQUIRED CHKS, FUEL, MIXTURE, THROTTLE, CARB HEAT, IGNITION, MASTER, AND PRIMER. ALL WERE IN PROPER PLACE. THE THROTTLE WAS CLOSED. AROUND 1000 MSL TO 1200 MSL, I INSTRUCTED STUDENT TO EXECUTE A GAR. THERE WAS NO PWR.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.