37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 256202 |
Time | |
Date | 199311 |
Day | Thu |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : dtw |
State Reference | MI |
Altitude | agl bound lower : 0 agl bound upper : 0 |
Environment | |
Flight Conditions | IMC |
Light | Daylight |
Aircraft 1 | |
Operator | common carrier : air carrier |
Make Model Name | Medium Transport, Low Wing, 2 Turboprop Eng |
Flight Phase | climbout : takeoff other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : atp |
Experience | flight time last 90 days : 100 flight time total : 3700 flight time type : 1000 |
ASRS Report | 256202 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Events | |
Anomaly | aircraft equipment problem : less severe non adherence : published procedure non adherence other other anomaly other |
Independent Detector | aircraft equipment other aircraft equipment : unspecified other flight crewa |
Resolutory Action | flight crew : rejected takeoff |
Consequence | Other |
Supplementary | |
Primary Problem | Flight Crew Human Performance |
Air Traffic Incident | Pilot Deviation |
Narrative:
Maintenance required a test flight on airplane for rudder vibrations. Captain's leg. Far 91 test flight. We took runway. Captain advanced power lever way too fast (almost firewall). Company operations says smooth application on takeoff at 60 percent, PNF sets takeoff power. Captain went to 100 percent very hard. As a result, engine started to bypass fuel out of can and surge. We aborted. Tower asked why. Captain said maintenance related. Captain decided to be an a&P and did his own static power check, this time with a smooth application of power. Operations checked good and we made power ok on takeoff #2. Problem: we aborted a takeoff. Captain did not write anything up in our maintenance log. If 'feds' investigated, there is no record of it. Captain erred big time!
Original NASA ASRS Text
Title: CAPT OF AN MDT ACR ACFT ABORTED TKOF DUE TO ENG FUEL SURGES.
Narrative: MAINT REQUIRED A TEST FLT ON AIRPLANE FOR RUDDER VIBRATIONS. CAPT'S LEG. FAR 91 TEST FLT. WE TOOK RWY. CAPT ADVANCED PWR LEVER WAY TOO FAST (ALMOST FIREWALL). COMPANY OPS SAYS SMOOTH APPLICATION ON TKOF AT 60 PERCENT, PNF SETS TKOF PWR. CAPT WENT TO 100 PERCENT VERY HARD. AS A RESULT, ENG STARTED TO BYPASS FUEL OUT OF CAN AND SURGE. WE ABORTED. TWR ASKED WHY. CAPT SAID MAINT RELATED. CAPT DECIDED TO BE AN A&P AND DID HIS OWN STATIC PWR CHK, THIS TIME WITH A SMOOTH APPLICATION OF PWR. OPS CHKED GOOD AND WE MADE PWR OK ON TKOF #2. PROB: WE ABORTED A TKOF. CAPT DID NOT WRITE ANYTHING UP IN OUR MAINT LOG. IF 'FEDS' INVESTIGATED, THERE IS NO RECORD OF IT. CAPT ERRED BIG TIME!
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.