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|
Attributes | |
ACN | 256596 |
Time | |
Date | 199311 |
Day | Sun |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : pia |
State Reference | IL |
Altitude | agl bound lower : 0 agl bound upper : 0 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Operator | common carrier : air carrier |
Make Model Name | Medium Transport, High Wing, 2 Turboprop Eng |
Navigation In Use | Other Other |
Flight Phase | other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : instrument pilot : commercial pilot : cfi pilot : atp |
Experience | flight time last 90 days : 100 flight time total : 3400 flight time type : 3300 |
ASRS Report | 256596 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : instrument pilot : commercial |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | aircraft equipment other aircraft equipment : unspecified other flight crewa |
Resolutory Action | flight crew : rejected takeoff flight crew : overcame equipment problem |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | other |
Narrative:
During takeoff roll, #2 ahrs failed, which caused attitude and heading reference loss on first officer side. Takeoff was immediately aborted. While taxiing to a spot to work on the problem, first officer tried the quick erect button the ahrs did not come back up -- but I don't believe my first officer kept the button depressed the complete 15 seconds. By this time, I had brought the aircraft to a complete stop at a spot we could wait out a system reboot. I pulled the #2 ahrs circuit breakers and the system came back indicating that it was in a proper 3 min initialization. I asked my first officer if he would be comfortable now continuing the flight. He said he would have been comfortable continuing without aborting! I let him know I disagreed -- that if it had occurred after V1, I would have continued to the hub, but not prior to V1. As far as I am concerned, this first officer's judgement exemplifies his experiences with other company capts. We discussed now continuing the flight, and agreed the system most likely was still just cold-soaked, and could not handle the 90 degree into position on the runway and took a second to fault.
Original NASA ASRS Text
Title: AN ACR MDT CREW ABORTED THEIR TKOF WHEN THE AHSI FAILED IN HDG.
Narrative: DURING TKOF ROLL, #2 AHRS FAILED, WHICH CAUSED ATTITUDE AND HDG REF LOSS ON FO SIDE. TKOF WAS IMMEDIATELY ABORTED. WHILE TAXIING TO A SPOT TO WORK ON THE PROB, FO TRIED THE QUICK ERECT BUTTON THE AHRS DID NOT COME BACK UP -- BUT I DON'T BELIEVE MY FO KEPT THE BUTTON DEPRESSED THE COMPLETE 15 SECONDS. BY THIS TIME, I HAD BROUGHT THE ACFT TO A COMPLETE STOP AT A SPOT WE COULD WAIT OUT A SYS REBOOT. I PULLED THE #2 AHRS CIRCUIT BREAKERS AND THE SYS CAME BACK INDICATING THAT IT WAS IN A PROPER 3 MIN INITIALIZATION. I ASKED MY FO IF HE WOULD BE COMFORTABLE NOW CONTINUING THE FLT. HE SAID HE WOULD HAVE BEEN COMFORTABLE CONTINUING WITHOUT ABORTING! I LET HIM KNOW I DISAGREED -- THAT IF IT HAD OCCURRED AFTER V1, I WOULD HAVE CONTINUED TO THE HUB, BUT NOT PRIOR TO V1. AS FAR AS I AM CONCERNED, THIS FO'S JUDGEMENT EXEMPLIFIES HIS EXPERIENCES WITH OTHER COMPANY CAPTS. WE DISCUSSED NOW CONTINUING THE FLT, AND AGREED THE SYS MOST LIKELY WAS STILL JUST COLD-SOAKED, AND COULD NOT HANDLE THE 90 DEG INTO POS ON THE RWY AND TOOK A SECOND TO FAULT.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.