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|
Attributes | |
ACN | 258756 |
Time | |
Date | 199312 |
Day | Mon |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : msp |
State Reference | MN |
Altitude | msl bound lower : 4000 msl bound upper : 4000 |
Environment | |
Flight Conditions | VMC |
Light | Night |
Aircraft 1 | |
Controlling Facilities | tower : msp |
Operator | common carrier : air carrier |
Make Model Name | Medium Large Transport, Low Wing, 2 Turbojet Eng |
Flight Phase | climbout : takeoff other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : private pilot : atp pilot : commercial pilot : flight engineer pilot : instrument |
Experience | flight time last 90 days : 220 flight time total : 13500 flight time type : 8000 |
ASRS Report | 258756 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : commercial pilot : instrument |
Events | |
Anomaly | aircraft equipment problem : less severe |
Independent Detector | other flight crewa other other : unspecified |
Resolutory Action | none taken : unable other |
Consequence | Other |
Supplementary | |
Air Traffic Incident | other |
Narrative:
After takeoff gear would not retract. Departure informed us transponder did not work. After further investigation, we discovered cabin would not pressurize, spoilers would not arm for landing -- all pointing to ground shift failure. The airplane had a gear problem on previous day and maintenance had corrected it. An overweight landing was made in accordance with directives and no further problems realized. Upon reaching the gate, the mechanic who met us informed us the ground shift mechanism was disconnected. Suspect maintenance had failed to connect after working on the gear.
Original NASA ASRS Text
Title: ACR MAINT FAILED TO REINSTATE THE GND SHIFT MECHANISM ON AN MLG.
Narrative: AFTER TKOF GEAR WOULD NOT RETRACT. DEP INFORMED US XPONDER DID NOT WORK. AFTER FURTHER INVESTIGATION, WE DISCOVERED CABIN WOULD NOT PRESSURIZE, SPOILERS WOULD NOT ARM FOR LNDG -- ALL POINTING TO GND SHIFT FAILURE. THE AIRPLANE HAD A GEAR PROB ON PREVIOUS DAY AND MAINT HAD CORRECTED IT. AN OVERWT LNDG WAS MADE IN ACCORDANCE WITH DIRECTIVES AND NO FURTHER PROBS REALIZED. UPON REACHING THE GATE, THE MECH WHO MET US INFORMED US THE GND SHIFT MECHANISM WAS DISCONNECTED. SUSPECT MAINT HAD FAILED TO CONNECT AFTER WORKING ON THE GEAR.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.