37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 273998 |
Time | |
Date | 199406 |
Day | Fri |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | atc facility : jax |
State Reference | FL |
Altitude | msl bound lower : 31000 msl bound upper : 31000 |
Aircraft 1 | |
Controlling Facilities | artcc : zjx |
Operator | common carrier : air carrier |
Make Model Name | B737 Undifferentiated or Other Model |
Operating Under FAR Part | Part 121 |
Flight Phase | cruise other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Experience | flight time last 90 days : 100 flight time total : 12300 flight time type : 1000 |
ASRS Report | 273998 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : commercial pilot : instrument pilot : atp |
Events | |
Anomaly | aircraft equipment problem : less severe non adherence : published procedure non adherence : far |
Independent Detector | other other : unspecified |
Resolutory Action | other |
Consequence | Other |
Supplementary | |
Primary Problem | Flight Crew Human Performance |
Air Traffic Incident | Pilot Deviation |
Narrative:
At 31000 ft I instructed first officer to go to cabin to inspect loose overhead panel. I did not immediately go to oxygen. First officer and I are reserve pilots. We were called to the airport with very little time to get there. Arrived 15 mins prior to scheduled departure. FAA air carrier inspector was waiting. Prepared aircraft (first officer arrived 5-10 mins prior to scheduled departure) and departed on schedule. Flight was short 57 mins atl-dab. On takeoff got warning lights for reverser lock problem. Climb out was busy avoiding broken cumulus clouds. Very busy talking to company reporting problem. At cruise flight attendant calls about overhead bin coming down on passenger. I instructed first officer to return to cabin and check. At this time I turned to watch FAA inspector go through the cumbersome process of getting out of jumpseat (B737). I should have immediately donned my oxygen mask. First officer had unbuckled his seat belt, turned sideways and also was watching FAA inspector. At this point inspector advised me to go on oxygen. I also had not flown for 3 weeks and first officer had not flown for 5 weeks. It was a very fast paced day with a lot of distrs and a slightly rusty crew.
Original NASA ASRS Text
Title: CAPT FAILS TO DON OXYGEN IMMEDIATELY WHEN FO LEAVES HIS SEAT.
Narrative: AT 31000 FT I INSTRUCTED FO TO GO TO CABIN TO INSPECT LOOSE OVERHEAD PANEL. I DID NOT IMMEDIATELY GO TO OXYGEN. FO AND I ARE RESERVE PLTS. WE WERE CALLED TO THE ARPT WITH VERY LITTLE TIME TO GET THERE. ARRIVED 15 MINS PRIOR TO SCHEDULED DEP. FAA ACR INSPECTOR WAS WAITING. PREPARED ACFT (FO ARRIVED 5-10 MINS PRIOR TO SCHEDULED DEP) AND DEPARTED ON SCHEDULE. FLT WAS SHORT 57 MINS ATL-DAB. ON TKOF GOT WARNING LIGHTS FOR REVERSER LOCK PROB. CLBOUT WAS BUSY AVOIDING BROKEN CUMULUS CLOUDS. VERY BUSY TALKING TO COMPANY RPTING PROB. AT CRUISE FLT ATTENDANT CALLS ABOUT OVERHEAD BIN COMING DOWN ON PAX. I INSTRUCTED FO TO RETURN TO CABIN AND CHK. AT THIS TIME I TURNED TO WATCH FAA INSPECTOR GO THROUGH THE CUMBERSOME PROCESS OF GETTING OUT OF JUMPSEAT (B737). I SHOULD HAVE IMMEDIATELY DONNED MY OXYGEN MASK. FO HAD UNBUCKLED HIS SEAT BELT, TURNED SIDEWAYS AND ALSO WAS WATCHING FAA INSPECTOR. AT THIS POINT INSPECTOR ADVISED ME TO GO ON OXYGEN. I ALSO HAD NOT FLOWN FOR 3 WKS AND FO HAD NOT FLOWN FOR 5 WKS. IT WAS A VERY FAST PACED DAY WITH A LOT OF DISTRS AND A SLIGHTLY RUSTY CREW.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.