37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 277651 |
Time | |
Date | 199407 |
Day | Sun |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : shv |
State Reference | LA |
Altitude | msl bound lower : 37000 msl bound upper : 37000 |
Environment | |
Flight Conditions | Mixed |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tower : shv |
Operator | common carrier : air carrier |
Make Model Name | Commercial Fixed Wing |
Operating Under FAR Part | Part 121 |
Navigation In Use | Other Other |
Flight Phase | climbout : takeoff other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Experience | flight time last 90 days : 150 flight time total : 15000 flight time type : 2000 |
ASRS Report | 277651 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : instrument pilot : commercial |
Events | |
Anomaly | aircraft equipment problem : critical |
Independent Detector | other flight crewa |
Resolutory Action | none taken : unable other |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | other |
Narrative:
After takeoff, first officer had to use override switch to raise the gear. Takeoff WX was 100 and 1. Air/ground sensing switch had not worked. After running all procedures and talking to maintenance, we continued and climbed to FL370. Pack cooling turbo fans overheated because they were still on since aircraft thought it was on ground. They caused smoke in cabin. We ran smoke removal checklist and then diverted to dfw. Our book procedures at airline X did not cover this problem well. It did not even tell us all of the system that were affected by the air/ground sensor. I'm working with my chief pilot to correct this.
Original NASA ASRS Text
Title: DIVERT LAND DUE TO GND SENSING SYS FAILURE.
Narrative: AFTER TKOF, FO HAD TO USE OVERRIDE SWITCH TO RAISE THE GEAR. TKOF WX WAS 100 AND 1. AIR/GND SENSING SWITCH HAD NOT WORKED. AFTER RUNNING ALL PROCS AND TALKING TO MAINT, WE CONTINUED AND CLBED TO FL370. PACK COOLING TURBO FANS OVERHEATED BECAUSE THEY WERE STILL ON SINCE ACFT THOUGHT IT WAS ON GND. THEY CAUSED SMOKE IN CABIN. WE RAN SMOKE REMOVAL CHKLIST AND THEN DIVERTED TO DFW. OUR BOOK PROCS AT AIRLINE X DID NOT COVER THIS PROB WELL. IT DID NOT EVEN TELL US ALL OF THE SYS THAT WERE AFFECTED BY THE AIR/GND SENSOR. I'M WORKING WITH MY CHIEF PLT TO CORRECT THIS.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.