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|
Attributes | |
ACN | 285753 |
Time | |
Date | 199410 |
Day | Mon |
Place | |
Locale Reference | airport : 9k4 |
State Reference | MO |
Altitude | agl bound lower : 0 agl bound upper : 600 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Operator | general aviation : instructional |
Make Model Name | Small Aircraft, Low Wing, 1 Eng, Retractable Gear |
Flight Phase | cruise other cruise other other |
Flight Plan | None |
Person 1 | |
Affiliation | Other |
Function | instruction : instructor |
Qualification | pilot : commercial pilot : cfi pilot : instrument |
Experience | flight time last 90 days : 250 flight time total : 1200 flight time type : 50 |
ASRS Report | 285753 |
Person 2 | |
Affiliation | Other |
Function | instruction : trainee |
Qualification | pilot : private |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | aircraft equipment other aircraft equipment : unspecified other flight crewa |
Resolutory Action | flight crew : declared emergency other |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Narrative:
Student and I were at an altitude of 500 ft AGL executing commercial ground reference maneuvers when the engine RPM increased despite the propeller control on the beech sierra. After a check of the oil pressure, or lack thereof, there was /0/ pressure and the decision to land was made. I took control of the aircraft, pulled the throttle to idle, executed a left 150 degree turn towards an acceptable field. In the turn the gear was extended and on short final, full flaps. We crossed a tree line by about 30 ft and landed in a pasture field. We stopped just short of a barbed wire fence and no damage was done to the aircraft other than the engine, which was still turning when we came to a complete stop. We pulled mixture and shut down engine. No injuries whatsoever. After taking the cowling off, we noticed that the oil screen bolt had backed out of the engine block because it was not safety-wired or properly torqued down. This situation could have been avoided if the mechanic had directly supervised the work done on the engine.
Original NASA ASRS Text
Title: LOSS OF ENG PWR DURING GND REF TRAINING MANEUVERS RESULTING IN A FORCED OFF ARPT LNDG.
Narrative: STUDENT AND I WERE AT AN ALT OF 500 FT AGL EXECUTING COMMERCIAL GND REF MANEUVERS WHEN THE ENG RPM INCREASED DESPITE THE PROP CTL ON THE BEECH SIERRA. AFTER A CHK OF THE OIL PRESSURE, OR LACK THEREOF, THERE WAS /0/ PRESSURE AND THE DECISION TO LAND WAS MADE. I TOOK CTL OF THE ACFT, PULLED THE THROTTLE TO IDLE, EXECUTED A L 150 DEG TURN TOWARDS AN ACCEPTABLE FIELD. IN THE TURN THE GEAR WAS EXTENDED AND ON SHORT FINAL, FULL FLAPS. WE CROSSED A TREE LINE BY ABOUT 30 FT AND LANDED IN A PASTURE FIELD. WE STOPPED JUST SHORT OF A BARBED WIRE FENCE AND NO DAMAGE WAS DONE TO THE ACFT OTHER THAN THE ENG, WHICH WAS STILL TURNING WHEN WE CAME TO A COMPLETE STOP. WE PULLED MIXTURE AND SHUT DOWN ENG. NO INJURIES WHATSOEVER. AFTER TAKING THE COWLING OFF, WE NOTICED THAT THE OIL SCREEN BOLT HAD BACKED OUT OF THE ENG BLOCK BECAUSE IT WAS NOT SAFETY-WIRED OR PROPERLY TORQUED DOWN. THIS SIT COULD HAVE BEEN AVOIDED IF THE MECH HAD DIRECTLY SUPERVISED THE WORK DONE ON THE ENG.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.