Narrative:

#1 engine/propeller went into automatic-feather at 100 percent torque, 100 ft AGL. Captain was non-flying pilot. I realized the problem and turned the system off. Engine indications returned to normal we did not shut the engine down. Made left traffic and landed runway 6L. No other incidents noted or observed. First officer did an outstanding job flying while I trouble shot the problem!

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Original NASA ASRS Text

Title: LTT HAD 1 ENG AUTO-FEATHER ON INITIAL CLB AFTER TKOF CAUSING THE FLC TO RETURN AND LAND.

Narrative: #1 ENG/PROP WENT INTO AUTO-FEATHER AT 100 PERCENT TORQUE, 100 FT AGL. CAPT WAS NON-FLYING PLT. I REALIZED THE PROB AND TURNED THE SYS OFF. ENG INDICATIONS RETURNED TO NORMAL WE DID NOT SHUT THE ENG DOWN. MADE L TFC AND LANDED RWY 6L. NO OTHER INCIDENTS NOTED OR OBSERVED. FO DID AN OUTSTANDING JOB FLYING WHILE I TROUBLE SHOT THE PROB!

Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.