37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 289094 |
Time | |
Date | 199411 |
Day | Sun |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : day |
State Reference | OH |
Altitude | agl bound lower : 100 agl bound upper : 100 |
Environment | |
Flight Conditions | VMC |
Light | Dawn |
Aircraft 1 | |
Controlling Facilities | tower : day |
Operator | common carrier : air carrier |
Make Model Name | Brasilia EMB-120 All Series |
Operating Under FAR Part | Part 135 |
Flight Phase | climbout : initial |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Experience | flight time last 90 days : 300 flight time total : 7000 flight time type : 3000 |
ASRS Report | 289094 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : instrument pilot : commercial |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | aircraft equipment other aircraft equipment : unspecified other flight crewa |
Resolutory Action | flight crew : declared emergency other |
Consequence | faa : investigated Other |
Supplementary | |
Primary Problem | Aircraft |
Narrative:
#1 engine/propeller went into automatic-feather at 100 percent torque, 100 ft AGL. Captain was non-flying pilot. I realized the problem and turned the system off. Engine indications returned to normal we did not shut the engine down. Made left traffic and landed runway 6L. No other incidents noted or observed. First officer did an outstanding job flying while I trouble shot the problem!
Original NASA ASRS Text
Title: LTT HAD 1 ENG AUTO-FEATHER ON INITIAL CLB AFTER TKOF CAUSING THE FLC TO RETURN AND LAND.
Narrative: #1 ENG/PROP WENT INTO AUTO-FEATHER AT 100 PERCENT TORQUE, 100 FT AGL. CAPT WAS NON-FLYING PLT. I REALIZED THE PROB AND TURNED THE SYS OFF. ENG INDICATIONS RETURNED TO NORMAL WE DID NOT SHUT THE ENG DOWN. MADE L TFC AND LANDED RWY 6L. NO OTHER INCIDENTS NOTED OR OBSERVED. FO DID AN OUTSTANDING JOB FLYING WHILE I TROUBLE SHOT THE PROB!
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.