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|
Attributes | |
ACN | 303554 |
Time | |
Date | 199505 |
Day | Wed |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | atc facility : buf airport : zob |
State Reference | NY |
Altitude | msl bound lower : 37000 msl bound upper : 37000 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Operator | common carrier : air carrier |
Make Model Name | Commercial Fixed Wing |
Operating Under FAR Part | Part 121 |
Navigation In Use | Other |
Flight Phase | cruise other descent : approach landing other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Experience | flight time last 90 days : 200 flight time total : 9000 flight time type : 2500 |
ASRS Report | 303554 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : atp |
Events | |
Anomaly | aircraft equipment problem : critical |
Independent Detector | other flight crewa |
Resolutory Action | none taken : unable |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | other |
Narrative:
#2 engine throttle was stuck at 92 percent. Talked to ZNY and advised the need to shut engine down prior to landing. Informed approach and tower of situation, asked for trucks (fire) to be standing by. Shut engine #2 down on short final and made uneventful landing. Suspect frozen water in cables. Callback conversation with reporter revealed the following information: postflt inspection of throttle cables revealed that the cables had grease on them and the takeoff in heavy rain caused moisture to collect on the greased cables. At the high altitude, cold temperature, the moisture froze rendering the throttle unmoveable. Even after remaining at a lower altitude, 10000 ft, for 20 mins, it still would not retard so on final approach was shut down. Finally, at the blocks, the flight crew was able to reduce the throttle. The aircraft was grounded and all cables were changed. The grease on the cables was apparently maintenance error.
Original NASA ASRS Text
Title: ACFT EQUIP PROB. FROZEN THROTTLE DUE TO IMPROPER MAINT.
Narrative: #2 ENG THROTTLE WAS STUCK AT 92 PERCENT. TALKED TO ZNY AND ADVISED THE NEED TO SHUT ENG DOWN PRIOR TO LNDG. INFORMED APCH AND TWR OF SIT, ASKED FOR TRUCKS (FIRE) TO BE STANDING BY. SHUT ENG #2 DOWN ON SHORT FINAL AND MADE UNEVENTFUL LNDG. SUSPECT FROZEN WATER IN CABLES. CALLBACK CONVERSATION WITH RPTR REVEALED THE FOLLOWING INFO: POSTFLT INSPECTION OF THROTTLE CABLES REVEALED THAT THE CABLES HAD GREASE ON THEM AND THE TKOF IN HVY RAIN CAUSED MOISTURE TO COLLECT ON THE GREASED CABLES. AT THE HIGH ALT, COLD TEMP, THE MOISTURE FROZE RENDERING THE THROTTLE UNMOVEABLE. EVEN AFTER REMAINING AT A LOWER ALT, 10000 FT, FOR 20 MINS, IT STILL WOULD NOT RETARD SO ON FINAL APCH WAS SHUT DOWN. FINALLY, AT THE BLOCKS, THE FLC WAS ABLE TO REDUCE THE THROTTLE. THE ACFT WAS GNDED AND ALL CABLES WERE CHANGED. THE GREASE ON THE CABLES WAS APPARENTLY MAINT ERROR.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.