37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 311801 |
Time | |
Date | 199507 |
Day | Wed |
Local Time Of Day | 0001 To 0600 |
Place | |
Locale Reference | atc facility : snn |
State Reference | FO |
Altitude | msl bound lower : 37000 msl bound upper : 37000 |
Environment | |
Flight Conditions | VMC |
Light | Dawn |
Aircraft 1 | |
Controlling Facilities | artcc : eggx |
Operator | common carrier : air carrier |
Make Model Name | L-1011 Tri-Star All Series |
Operating Under FAR Part | Part 121 |
Navigation In Use | Other |
Flight Phase | cruise other other |
Route In Use | enroute : other oceanic enroute : atlantic |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Experience | flight time last 90 days : 200 flight time total : 10000 flight time type : 2000 |
ASRS Report | 311801 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : commercial pilot : instrument |
Events | |
Anomaly | aircraft equipment problem : critical other spatial deviation |
Independent Detector | aircraft equipment other aircraft equipment : unspecified other flight crewa |
Resolutory Action | aircraft : equipment problem dissipated flight crew : overcame equipment problem |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | other |
Narrative:
At 25 mi west in the minneapolis area at FL370, #1 engine rolled back to idle. Exited track in accordance with with mnps procedures. Later determined engine had failed but with no cockpit indications. ATC cleared us to FL280 for relight. Restarted to idle only. Crew proceeded to snn because engine responded to idle only. Company requested to fly to lgw. While en route to lgw, engine then responded to normal inputs. Crew contacted company and with our concurrence, decided to fly to destination (ory) with engine normal. We rejoined our flight plan over landsend, received direct din. Then flight plan route. Flight remained normal until approach when #1 engine failed again on short approach. Landed normally with no event. Ory maintenance later determined reason for engine failure was a bad fuel regulator.
Original NASA ASRS Text
Title: PARTIAL ENG FAILURE OVER THE N ATLANTIC.
Narrative: AT 25 MI W IN THE MINNEAPOLIS AREA AT FL370, #1 ENG ROLLED BACK TO IDLE. EXITED TRACK IAW WITH MNPS PROCS. LATER DETERMINED ENG HAD FAILED BUT WITH NO COCKPIT INDICATIONS. ATC CLRED US TO FL280 FOR RELIGHT. RESTARTED TO IDLE ONLY. CREW PROCEEDED TO SNN BECAUSE ENG RESPONDED TO IDLE ONLY. COMPANY REQUESTED TO FLY TO LGW. WHILE ENRTE TO LGW, ENG THEN RESPONDED TO NORMAL INPUTS. CREW CONTACTED COMPANY AND WITH OUR CONCURRENCE, DECIDED TO FLY TO DEST (ORY) WITH ENG NORMAL. WE REJOINED OUR FLT PLAN OVER LANDSEND, RECEIVED DIRECT DIN. THEN FLT PLAN RTE. FLT REMAINED NORMAL UNTIL APCH WHEN #1 ENG FAILED AGAIN ON SHORT APCH. LANDED NORMALLY WITH NO EVENT. ORY MAINT LATER DETERMINED REASON FOR ENG FAILURE WAS A BAD FUEL REGULATOR.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.