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|
Attributes | |
ACN | 312672 |
Time | |
Date | 199508 |
Day | Tue |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | airport : dfw |
State Reference | TX |
Altitude | msl bound lower : 33000 msl bound upper : 33000 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | artcc : zfw |
Operator | common carrier : air carrier |
Make Model Name | MD-80 Super 80 |
Operating Under FAR Part | Part 121 |
Navigation In Use | Other |
Flight Phase | cruise other other other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : instrument pilot : commercial pilot : atp |
Experience | flight time last 90 days : 225 flight time total : 11000 flight time type : 3000 |
ASRS Report | 312672 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : atp |
Experience | flight time last 90 days : 280 flight time total : 10000 flight time type : 5000 |
ASRS Report | 313239 |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | aircraft equipment other aircraft equipment : unspecified other flight crewa |
Resolutory Action | flight crew : declared emergency other |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | other |
Narrative:
At cruise, 15 mins after fuel gauge indications were checked indicating normal quantity and balanced tanks, a 5000 pound imbalance and 5000 pound below planned quantity indication was noted. A quick check of fuel used gauges, timing of fuel quantity decrease for 1 min and noting a lateral out of trim condition all but confirmed a fuel leak. Normal fuel consumption would be plus or minus 100 pounds/min. We were using plus or minus 300 pounds/min. At this rate of consumption, we had no more than 25 mins of fuel remaining. Declared an emergency with center and requested immediate descent into dfw. Planned destination was iah. After initiating descent, called first flight attendant to cockpit and advised her of situation and the plan, ie, to make a normal landing at dfw in approximately 15 mins due to a possible fuel leak. Asked her to brief other flight attendants and to make a PA informing the customers. After completing necessary communications with ATC and company, and completing appropriate checklists, I made a PA to customers informing them that we were descending for a normal landing at dfw. I advised them to expect fire trucks to approach the aircraft after landing. We made a full flap idle reverse landing. On final approach, a commuter aircraft in front of us was sent around by tower as we were closing rapidly on him. As we crossed the approach lights an air carrier waiting for takeoff advised on tower frequency we had 'fuel pouring out of #1 engine.' in retrospect, I should not have even deployed the reversers. It did not cause us a problem, but it did blow fuel forward over the engine. I stopped the aircraft on the high speed, shutdown both engines, and did not start APU. Fire department foamed #1 engine and fuel on the ramp. No fire occurred. Customers deplaned without incident via aft air stairs (rather then risk injuries by use of evacuate/evacuation slides). Problem turned out to be a high pressure fuel line fitting that had blown out. Maybe had been over torqued??? We landed with 6-7 mins fuel remaining. All is well that ends well! Callback conversation with reporter revealed the following information: this flight crew was flying an md- 80, and the fuel leak was in the high-pressure line to the engine. The captain said that they considered shutting down the left engine to see if that would stop the left side leak, but decided against this course of action. They were worried that if the leak did not stop, they would then be in an unbalanced aircraft with only 1 engine. The crew went through the same type of decision path when considering to evacuate/evacuation or use the aft exit stairs. The stairs were used since there was no fire reported by the fire/rescue team, so the orderly, but rapid deplaning was done by use of the aft air stairs. There were no injuries. The passenger were sent on to their destination on other aircraft and the flight crew sent to a hotel. The next morning the flight crew picked up the repaired aircraft and resumed revenue service.
Original NASA ASRS Text
Title: ACFT EQUIP PROB -- EMER DECLARED ACR HAS A SEVERE HIGH- PRESSURE FUEL LEAK AND DIVERTS AND MAKES AN EXPEDITIOUS LNDG.
Narrative: AT CRUISE, 15 MINS AFTER FUEL GAUGE INDICATIONS WERE CHKED INDICATING NORMAL QUANTITY AND BALANCED TANKS, A 5000 LB IMBALANCE AND 5000 LB BELOW PLANNED QUANTITY INDICATION WAS NOTED. A QUICK CHK OF FUEL USED GAUGES, TIMING OF FUEL QUANTITY DECREASE FOR 1 MIN AND NOTING A LATERAL OUT OF TRIM CONDITION ALL BUT CONFIRMED A FUEL LEAK. NORMAL FUEL CONSUMPTION WOULD BE PLUS OR MINUS 100 LBS/MIN. WE WERE USING PLUS OR MINUS 300 LBS/MIN. AT THIS RATE OF CONSUMPTION, WE HAD NO MORE THAN 25 MINS OF FUEL REMAINING. DECLARED AN EMER WITH CTR AND REQUESTED IMMEDIATE DSCNT INTO DFW. PLANNED DEST WAS IAH. AFTER INITIATING DSCNT, CALLED FIRST FLT ATTENDANT TO COCKPIT AND ADVISED HER OF SIT AND THE PLAN, IE, TO MAKE A NORMAL LNDG AT DFW IN APPROX 15 MINS DUE TO A POSSIBLE FUEL LEAK. ASKED HER TO BRIEF OTHER FLT ATTENDANTS AND TO MAKE A PA INFORMING THE CUSTOMERS. AFTER COMPLETING NECESSARY COMS WITH ATC AND COMPANY, AND COMPLETING APPROPRIATE CHKLISTS, I MADE A PA TO CUSTOMERS INFORMING THEM THAT WE WERE DSNDING FOR A NORMAL LNDG AT DFW. I ADVISED THEM TO EXPECT FIRE TRUCKS TO APCH THE ACFT AFTER LNDG. WE MADE A FULL FLAP IDLE REVERSE LNDG. ON FINAL APCH, A COMMUTER ACFT IN FRONT OF US WAS SENT AROUND BY TWR AS WE WERE CLOSING RAPIDLY ON HIM. AS WE CROSSED THE APCH LIGHTS AN ACR WAITING FOR TKOF ADVISED ON TWR FREQ WE HAD 'FUEL POURING OUT OF #1 ENG.' IN RETROSPECT, I SHOULD NOT HAVE EVEN DEPLOYED THE REVERSERS. IT DID NOT CAUSE US A PROB, BUT IT DID BLOW FUEL FORWARD OVER THE ENG. I STOPPED THE ACFT ON THE HIGH SPD, SHUTDOWN BOTH ENGS, AND DID NOT START APU. FIRE DEPT FOAMED #1 ENG AND FUEL ON THE RAMP. NO FIRE OCCURRED. CUSTOMERS DEPLANED WITHOUT INCIDENT VIA AFT AIR STAIRS (RATHER THEN RISK INJURIES BY USE OF EVAC SLIDES). PROB TURNED OUT TO BE A HIGH PRESSURE FUEL LINE FITTING THAT HAD BLOWN OUT. MAYBE HAD BEEN OVER TORQUED??? WE LANDED WITH 6-7 MINS FUEL REMAINING. ALL IS WELL THAT ENDS WELL! CALLBACK CONVERSATION WITH RPTR REVEALED THE FOLLOWING INFO: THIS FLC WAS FLYING AN MD- 80, AND THE FUEL LEAK WAS IN THE HIGH-PRESSURE LINE TO THE ENG. THE CAPT SAID THAT THEY CONSIDERED SHUTTING DOWN THE L ENG TO SEE IF THAT WOULD STOP THE L SIDE LEAK, BUT DECIDED AGAINST THIS COURSE OF ACTION. THEY WERE WORRIED THAT IF THE LEAK DID NOT STOP, THEY WOULD THEN BE IN AN UNBALANCED ACFT WITH ONLY 1 ENG. THE CREW WENT THROUGH THE SAME TYPE OF DECISION PATH WHEN CONSIDERING TO EVAC OR USE THE AFT EXIT STAIRS. THE STAIRS WERE USED SINCE THERE WAS NO FIRE RPTED BY THE FIRE/RESCUE TEAM, SO THE ORDERLY, BUT RAPID DEPLANING WAS DONE BY USE OF THE AFT AIR STAIRS. THERE WERE NO INJURIES. THE PAX WERE SENT ON TO THEIR DEST ON OTHER ACFT AND THE FLC SENT TO A HOTEL. THE NEXT MORNING THE FLC PICKED UP THE REPAIRED ACFT AND RESUMED REVENUE SVC.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.