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|
Attributes | |
ACN | 312784 |
Time | |
Date | 199508 |
Day | Mon |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | airport : szp |
State Reference | CA |
Altitude | msl bound lower : 2500 msl bound upper : 2500 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Operator | general aviation : personal |
Make Model Name | Cessna 170 |
Operating Under FAR Part | Part 91 |
Flight Phase | cruise other |
Flight Plan | VFR |
Person 1 | |
Affiliation | Other |
Function | flight crew : single pilot |
Qualification | pilot : private |
Experience | flight time last 90 days : 15 flight time total : 2500 flight time type : 1100 |
ASRS Report | 312784 |
Person 2 | |
Experience | flight time last 90 days : 15 flight time total : 2500 flight time type : 1100 |
Events | |
Anomaly | aircraft equipment problem : critical non adherence : far other anomaly other |
Independent Detector | aircraft equipment other aircraft equipment : unspecified |
Resolutory Action | flight crew : declared emergency none taken : unable |
Consequence | faa : investigated |
Supplementary | |
Primary Problem | Flight Crew Human Performance |
Air Traffic Incident | Pilot Deviation |
Narrative:
Aircraft was signed off from annual inspection aug/sun/95. I was flying past santa paula airport heading about 260 degrees, was approximately 2 mi west of airport when I decided to lean aircraft out. As soon as I touched mixture control engine stopped. I pushed mixture control in but engine only idled and eventually stopped completely. I contacted santa paula, advised them I was inbound with dead engine. Landing was uneventful. No damage to anything or anyone. Aircraft was checked over by mechanic and flown home no further problem. Callback conversation with reporter revealed the following information: it was just coincidental that, when adjusting the mixture control, the engine quit. The reporter pilot had failed to check the gas level on preflight and simply ran out of gas. He was close enough to the airport to dead stick it in. 'Very embarrassing,' said the reporter because everyone stopped and watched, then had to help him push the aircraft off the runway.
Original NASA ASRS Text
Title: RAN OUT OF GAS.
Narrative: ACFT WAS SIGNED OFF FROM ANNUAL INSPECTION AUG/SUN/95. I WAS FLYING PAST SANTA PAULA ARPT HEADING ABOUT 260 DEGS, WAS APPROX 2 MI W OF ARPT WHEN I DECIDED TO LEAN ACFT OUT. AS SOON AS I TOUCHED MIXTURE CTL ENG STOPPED. I PUSHED MIXTURE CTL IN BUT ENG ONLY IDLED AND EVENTUALLY STOPPED COMPLETELY. I CONTACTED SANTA PAULA, ADVISED THEM I WAS INBOUND WITH DEAD ENG. LNDG WAS UNEVENTFUL. NO DAMAGE TO ANYTHING OR ANYONE. ACFT WAS CHKED OVER BY MECH AND FLOWN HOME NO FURTHER PROB. CALLBACK CONVERSATION WITH RPTR REVEALED THE FOLLOWING INFO: IT WAS JUST COINCIDENTAL THAT, WHEN ADJUSTING THE MIXTURE CTL, THE ENG QUIT. THE RPTR PLT HAD FAILED TO CHK THE GAS LEVEL ON PREFLT AND SIMPLY RAN OUT OF GAS. HE WAS CLOSE ENOUGH TO THE ARPT TO DEAD STICK IT IN. 'VERY EMBARRASSING,' SAID THE RPTR BECAUSE EVERYONE STOPPED AND WATCHED, THEN HAD TO HELP HIM PUSH THE ACFT OFF THE RWY.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.