37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 324466 |
Time | |
Date | 199512 |
Day | Tue |
Local Time Of Day | 1801 To 2400 |
Place | |
Locale Reference | airport : mke |
State Reference | WI |
Altitude | msl bound lower : 39000 msl bound upper : 39000 |
Environment | |
Flight Conditions | VMC |
Light | Night |
Aircraft 1 | |
Controlling Facilities | artcc : zau tracon : mke tower : tpa |
Operator | common carrier : air carrier |
Make Model Name | Any Unknown or Unlisted Aircraft Manufacturer |
Operating Under FAR Part | Part 91 |
Navigation In Use | Other Other |
Flight Phase | descent other |
Route In Use | arrival other arrival star : star |
Flight Plan | IFR |
Person 1 | |
Affiliation | Other |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Experience | flight time last 90 days : 60 flight time total : 11000 flight time type : 1000 |
ASRS Report | 324466 |
Person 2 | |
Affiliation | Other |
Function | flight crew : first officer |
Qualification | pilot : commercial pilot : instrument |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | aircraft equipment other aircraft equipment : unspecified other flight crewa |
Resolutory Action | flight crew : declared emergency other other |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | other |
Narrative:
Soon after starting an autothrottle VNAV descent on a STAR into dtw from oma, a vibration was felt throughout the airplane. The left engine turbine gas temperature was climbing toward 700 degrees and the fuel flow/hp/lp were all at normal VNAV readings. The left throttle was taken off autothrottle and reduced to idle. The turbine gas temperature stayed high. The engine was shut down. A coordinated change of destination was done through ATC to make a single-engine (uneventful) landing at mke. The fault was found to be a bad engine air control actuator. ATC and mke approach/tower coordination was professional and flawless.
Original NASA ASRS Text
Title: FLC OF AN MLG DIVERTED TO LAND AFTER SHUTTING DOWN 1 ENG DUE TO A FAULTY FUEL CTLR.
Narrative: SOON AFTER STARTING AN AUTOTHROTTLE VNAV DSCNT ON A STAR INTO DTW FROM OMA, A VIBRATION WAS FELT THROUGHOUT THE AIRPLANE. THE L ENG TURBINE GAS TEMP WAS CLBING TOWARD 700 DEGS AND THE FUEL FLOW/HP/LP WERE ALL AT NORMAL VNAV READINGS. THE L THROTTLE WAS TAKEN OFF AUTOTHROTTLE AND REDUCED TO IDLE. THE TURBINE GAS TEMP STAYED HIGH. THE ENG WAS SHUT DOWN. A COORDINATED CHANGE OF DEST WAS DONE THROUGH ATC TO MAKE A SINGLE-ENG (UNEVENTFUL) LNDG AT MKE. THE FAULT WAS FOUND TO BE A BAD ENG AIR CTL ACTUATOR. ATC AND MKE APCH/TWR COORD WAS PROFESSIONAL AND FLAWLESS.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.