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|
Attributes | |
ACN | 327411 |
Time | |
Date | 199601 |
Day | Sun |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : ord |
State Reference | IL |
Altitude | agl bound lower : 0 agl bound upper : 0 |
Environment | |
Flight Conditions | VMC |
Light | Dawn |
Aircraft 1 | |
Controlling Facilities | artcc : zbw |
Operator | common carrier : air carrier |
Make Model Name | MD-83 |
Operating Under FAR Part | Part 121 |
Navigation In Use | Other Other |
Flight Phase | climbout : takeoff ground : preflight ground other : taxi |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Experience | flight time last 90 days : 210 flight time total : 9000 flight time type : 5700 |
ASRS Report | 327411 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : instrument pilot : commercial |
Events | |
Anomaly | aircraft equipment problem : less severe |
Independent Detector | other other : unspecified |
Resolutory Action | none taken : detected after the fact |
Consequence | other |
Supplementary | |
Air Traffic Incident | other |
Narrative:
Pushed back from gate at ord with an air carrier B727 right next to us. We were pushed straight back out of gate and the tug started to turn us to face our nose out toward txwys. Tug stopped with nose cocked 90 degrees to the right. At that point I was told to set brakes. With nosewheel cocked to right and the B727 in front of us, I set brakes and specifically asked for wing walker to clear the air carrier. We were disconnected, shown the pin and the crew was gone, walking away with their backs toward us. We carefully made the turnout without wing walkers. Flight was uneventful and arrived early to cun. On arrival ground handler came up to cockpit as we deplaned and told us that our aircraft was damaged. Large dent in tail. We knew we did not hit anything in cun. I went out to look and it was obvious why ord crew stopped pushback where they did, and why they didn't stay to walk wing by the air carrier B727. It is this crew's opinion that the pushback crew knew what they did and were aware of the strike -- that is why they stopped us at the odd angle and left as soon as possible. I don't believe the crew looked for or cared about damage to our aircraft. They just feared for their jobs. This is negligent and put crew and passenger in possible danger. Preliminary interviews with ground crew shows that wing walkers thought we hit fence and told crew chief, but he said he didn't hit anything. My concern is that he allowed us to take off with substantial tailcone damage and not looking or advising this crew of it. I was told that this ground crew was terminated. Aircraft was an MD83. Callback conversation with reporter revealed the following information: the tailcone skin was dented and torn 6 inches below rudder section. The flight crew noticed nothing unusual during their 4 hour flight to cancun, except 1/2 notch of rudder trim. The mechanic who repaired the aircraft told the captain that they were fortunate as the tail could have been aerodynamically ripped off, in-flight, with this type of damage. In a congested gate area, the MD83 had been pushed into a cement blast fence with chain link on top. The tail section skin was torn and dented from the chain link fence. One of the wing walkers had crossed wands when contact with the fence was imminent, but the tug driver failed to see the signal. When the wing walker told him of the damage, he did not respond. He was fired for his negligence.
Original NASA ASRS Text
Title: AN ACR MD83 WAS DAMAGED DURING PUSHBACK. FLC WAS NOT TOLD THAT THE ACFT WAS DAMAGED. FLT DEPARTED AND DAMAGE WAS NOT DISCOVERED UNTIL ARR AT THE DEST, BY GND PERSONNEL.
Narrative: PUSHED BACK FROM GATE AT ORD WITH AN ACR B727 RIGHT NEXT TO US. WE WERE PUSHED STRAIGHT BACK OUT OF GATE AND THE TUG STARTED TO TURN US TO FACE OUR NOSE OUT TOWARD TXWYS. TUG STOPPED WITH NOSE COCKED 90 DEGS TO THE R. AT THAT POINT I WAS TOLD TO SET BRAKES. WITH NOSEWHEEL COCKED TO R AND THE B727 IN FRONT OF US, I SET BRAKES AND SPECIFICALLY ASKED FOR WING WALKER TO CLR THE ACR. WE WERE DISCONNECTED, SHOWN THE PIN AND THE CREW WAS GONE, WALKING AWAY WITH THEIR BACKS TOWARD US. WE CAREFULLY MADE THE TURNOUT WITHOUT WING WALKERS. FLT WAS UNEVENTFUL AND ARRIVED EARLY TO CUN. ON ARR GND HANDLER CAME UP TO COCKPIT AS WE DEPLANED AND TOLD US THAT OUR ACFT WAS DAMAGED. LARGE DENT IN TAIL. WE KNEW WE DID NOT HIT ANYTHING IN CUN. I WENT OUT TO LOOK AND IT WAS OBVIOUS WHY ORD CREW STOPPED PUSHBACK WHERE THEY DID, AND WHY THEY DIDN'T STAY TO WALK WING BY THE ACR B727. IT IS THIS CREW'S OPINION THAT THE PUSHBACK CREW KNEW WHAT THEY DID AND WERE AWARE OF THE STRIKE -- THAT IS WHY THEY STOPPED US AT THE ODD ANGLE AND LEFT ASAP. I DON'T BELIEVE THE CREW LOOKED FOR OR CARED ABOUT DAMAGE TO OUR ACFT. THEY JUST FEARED FOR THEIR JOBS. THIS IS NEGLIGENT AND PUT CREW AND PAX IN POSSIBLE DANGER. PRELIMINARY INTERVIEWS WITH GND CREW SHOWS THAT WING WALKERS THOUGHT WE HIT FENCE AND TOLD CREW CHIEF, BUT HE SAID HE DIDN'T HIT ANYTHING. MY CONCERN IS THAT HE ALLOWED US TO TAKE OFF WITH SUBSTANTIAL TAILCONE DAMAGE AND NOT LOOKING OR ADVISING THIS CREW OF IT. I WAS TOLD THAT THIS GND CREW WAS TERMINATED. ACFT WAS AN MD83. CALLBACK CONVERSATION WITH RPTR REVEALED THE FOLLOWING INFO: THE TAILCONE SKIN WAS DENTED AND TORN 6 INCHES BELOW RUDDER SECTION. THE FLC NOTICED NOTHING UNUSUAL DURING THEIR 4 HR FLT TO CANCUN, EXCEPT 1/2 NOTCH OF RUDDER TRIM. THE MECH WHO REPAIRED THE ACFT TOLD THE CAPT THAT THEY WERE FORTUNATE AS THE TAIL COULD HAVE BEEN AERODYNAMICALLY RIPPED OFF, INFLT, WITH THIS TYPE OF DAMAGE. IN A CONGESTED GATE AREA, THE MD83 HAD BEEN PUSHED INTO A CEMENT BLAST FENCE WITH CHAIN LINK ON TOP. THE TAIL SECTION SKIN WAS TORN AND DENTED FROM THE CHAIN LINK FENCE. ONE OF THE WING WALKERS HAD CROSSED WANDS WHEN CONTACT WITH THE FENCE WAS IMMINENT, BUT THE TUG DRIVER FAILED TO SEE THE SIGNAL. WHEN THE WING WALKER TOLD HIM OF THE DAMAGE, HE DID NOT RESPOND. HE WAS FIRED FOR HIS NEGLIGENCE.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.