37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 339136 |
Time | |
Date | 199606 |
Day | Sun |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : ont |
State Reference | CA |
Altitude | agl bound lower : 0 agl bound upper : 0 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Operator | common carrier : air carrier |
Make Model Name | Commercial Fixed Wing |
Operating Under FAR Part | Part 121 |
Navigation In Use | Other Other |
Flight Phase | ground : preflight |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : atp pilot : commercial |
Experience | flight time last 90 days : 250 flight time total : 5000 flight time type : 450 |
ASRS Report | 339136 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Events | |
Anomaly | aircraft equipment problem : less severe other anomaly other |
Independent Detector | other flight crewa |
Resolutory Action | none taken : detected after the fact |
Consequence | Other |
Supplementary | |
Primary Problem | Flight Crew Human Performance |
Air Traffic Incident | Pilot Deviation |
Narrative:
During my preflight inspection I came across the external power receptacle door and noticed that the ground crew had already set up for push back. Their headset was plugged in with the electrical cord hanging in front of the receptacle and the headset and mouth piece were hanging/resting on top of the partially open door. My checklist calls for me T open the door, check a communication switch and close the door. Since the crew wa already set up to push, I left the door set up as it was, and did not notice anything else abnormal at that time. Our originating flight was uneventful from ontario to phoenix. Upon arrival we were met by another crew for an aircraft swap out. The new first officer noticed a small crack in the skin of the aircraft just aft of the external power receptacle door. (The door closed at this time) the crew had maintenance check it and they found more extensive damage to the power receptacle itself and the wiring behind the door and into the fuselage! The aircraft was removed from service for repairs! Had I moved the headset and communications cord and made sure the door closed and latched properly, I might have noticed the damage to the skin and the damage to the power cord receptacle before our flight and avoided someone else discovering it for us after! As for why the guys who handled our push back on the tug and on the headset and why they did not inform the captain, or I, or maintenance either, I do not know. As for me, from now on just because things appear normal, that doesn't mean they are! Be vigilant, be thorough, and don't assume others are doing it for you! Needless to say, the incident is under investigation and the results will come out. It is suspected that the external power cart was towed away while still connected to the external power receptacle damaging the skin and the internal components.
Original NASA ASRS Text
Title: MLG FO DOING PREFLT INSPECTION FAILS TO CHK THE EXTERNAL PWR RECEPTACLE DOOR DUE TO HEADSET HANGING ON THE DOOR AND CORD HANGING OUT FROM IT. ON ACFT SWITCH SECOND FLC PREFLT SHOWED DAMAGE T THE SKIN AFT OF THE DOOR.
Narrative: DURING MY PREFLT INSPECTION I CAME ACROSS THE EXTERNAL PWR RECEPTACLE DOOR AND NOTICED THAT THE GND CREW HAD ALREADY SET UP FOR PUSH BACK. THEIR HEADSET WAS PLUGGED IN WITH THE ELECTRICAL CORD HANGING IN FRONT OF THE RECEPTACLE AND THE HEADSET AND MOUTH PIECE WERE HANGING/RESTING ON TOP OF THE PARTIALLY OPEN DOOR. MY CHKLIST CALLS FOR ME T OPEN THE DOOR, CHK A COM SWITCH AND CLOSE THE DOOR. SINCE THE CREW WA ALREADY SET UP TO PUSH, I LEFT THE DOOR SET UP AS IT WAS, AND DID NOT NOTICE ANYTHING ELSE ABNORMAL AT THAT TIME. OUR ORIGINATING FLT WAS UNEVENTFUL FROM ONTARIO TO PHOENIX. UPON ARR WE WERE MET BY ANOTHER CREW FOR AN ACFT SWAP OUT. THE NEW FO NOTICED A SMALL CRACK IN THE SKIN OF THE ACFT JUST AFT OF THE EXTERNAL PWR RECEPTACLE DOOR. (THE DOOR CLOSED AT THIS TIME) THE CREW HAD MAINT CHK IT AND THEY FOUND MORE EXTENSIVE DAMAGE TO THE PWR RECEPTACLE ITSELF AND THE WIRING BEHIND THE DOOR AND INTO THE FUSELAGE! THE ACFT WAS REMOVED FROM SVC FOR REPAIRS! HAD I MOVED THE HEADSET AND COMS CORD AND MADE SURE THE DOOR CLOSED AND LATCHED PROPERLY, I MIGHT HAVE NOTICED THE DAMAGE TO THE SKIN AND THE DAMAGE TO THE PWR CORD RECEPTACLE BEFORE OUR FLT AND AVOIDED SOMEONE ELSE DISCOVERING IT FOR US AFTER! AS FOR WHY THE GUYS WHO HANDLED OUR PUSH BACK ON THE TUG AND ON THE HEADSET AND WHY THEY DID NOT INFORM THE CAPT, OR I, OR MAINT EITHER, I DO NOT KNOW. AS FOR ME, FROM NOW ON JUST BECAUSE THINGS APPEAR NORMAL, THAT DOESN'T MEAN THEY ARE! BE VIGILANT, BE THOROUGH, AND DON'T ASSUME OTHERS ARE DOING IT FOR YOU! NEEDLESS TO SAY, THE INCIDENT IS UNDER INVESTIGATION AND THE RESULTS WILL COME OUT. IT IS SUSPECTED THAT THE EXTERNAL PWR CART WAS TOWED AWAY WHILE STILL CONNECTED TO THE EXTERNAL PWR RECEPTACLE DAMAGING THE SKIN AND THE INTERNAL COMPONENTS.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.