37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 339226 |
Time | |
Date | 199606 |
Day | Sat |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | atc facility : dab |
State Reference | FL |
Altitude | msl bound lower : 35000 msl bound upper : 35000 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | artcc : zjx |
Operator | common carrier : air carrier |
Make Model Name | Commercial Fixed Wing |
Operating Under FAR Part | Part 121 |
Flight Phase | cruise other descent other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : second officer |
Qualification | pilot : atp pilot : flight engineer |
Experience | flight time last 90 days : 150 flight time total : 4000 flight time type : 650 |
ASRS Report | 339226 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Events | |
Anomaly | aircraft equipment problem : less severe other anomaly other |
Independent Detector | other flight crewa other other : unspecified |
Resolutory Action | none taken : detected after the fact |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | Pilot Deviation other |
Narrative:
After starting initial descent into dab, we heard a rather loud thump. All aircraft system were normal we thought a wheelchair in the belly had fallen over. After a normal approach and landing, I did a quick exterior walkaround and noted no problems, tires and wings. We had a constant speed drive problem for maintenance to fix so I planned to do a thorough preflight after maintenance was done. While waiting on maintenance, ground personnel came up to the cockpit and said that we had a exterior panel missing under the aircraft and a small door was open. Upon inspection, we found a 2 ft by 3 ft air conditioning service door missing in front of the wheelwell. Also a small radio antenna access door was open. This appeared to be the thump we heard in flight (1 1/2 hours after takeoff) since baggage handlers said the wheelchair was stowed properly when they took it out. It was determined maintenance had been done on the aircraft overnight and a placard for a pack door inoperative had been removed. On my preflight, all doors and panels were up and appeared locked, but it seems maintenance must not have secured the doors properly. I know I did a good preflight because we had a dedicated mechanic to launch the aircraft and I found a loose light bulb in the right navigation lights that he removed. The panel blew off when we changed pitch and power for descent. Maintenance probably did not inspect the panel good enough when the work was done at night. I was on reserve and received a XX05 all for a XC20 show, XC20 push. 2 forward latches were undone on the opposite door. It was possible I could have missed them. The other door had screw fasteners and could be closed without knowing the door was secured.
Original NASA ASRS Text
Title: ACFT EQUIP PROB. EXTERIOR ACCESS PANEL CAME OFF INFLT AND A SMALL DOOR OPENED. ACFT HAD MAINT PRIOR TO FLT.
Narrative: AFTER STARTING INITIAL DSCNT INTO DAB, WE HEARD A RATHER LOUD THUMP. ALL ACFT SYS WERE NORMAL WE THOUGHT A WHEELCHAIR IN THE BELLY HAD FALLEN OVER. AFTER A NORMAL APCH AND LNDG, I DID A QUICK EXTERIOR WALKAROUND AND NOTED NO PROBS, TIRES AND WINGS. WE HAD A CONSTANT SPD DRIVE PROB FOR MAINT TO FIX SO I PLANNED TO DO A THOROUGH PREFLT AFTER MAINT WAS DONE. WHILE WAITING ON MAINT, GND PERSONNEL CAME UP TO THE COCKPIT AND SAID THAT WE HAD A EXTERIOR PANEL MISSING UNDER THE ACFT AND A SMALL DOOR WAS OPEN. UPON INSPECTION, WE FOUND A 2 FT BY 3 FT AIR CONDITIONING SVC DOOR MISSING IN FRONT OF THE WHEELWELL. ALSO A SMALL RADIO ANTENNA ACCESS DOOR WAS OPEN. THIS APPEARED TO BE THE THUMP WE HEARD IN FLT (1 1/2 HRS AFTER TKOF) SINCE BAGGAGE HANDLERS SAID THE WHEELCHAIR WAS STOWED PROPERLY WHEN THEY TOOK IT OUT. IT WAS DETERMINED MAINT HAD BEEN DONE ON THE ACFT OVERNIGHT AND A PLACARD FOR A PACK DOOR INOP HAD BEEN REMOVED. ON MY PREFLT, ALL DOORS AND PANELS WERE UP AND APPEARED LOCKED, BUT IT SEEMS MAINT MUST NOT HAVE SECURED THE DOORS PROPERLY. I KNOW I DID A GOOD PREFLT BECAUSE WE HAD A DEDICATED MECH TO LAUNCH THE ACFT AND I FOUND A LOOSE LIGHT BULB IN THE R NAV LIGHTS THAT HE REMOVED. THE PANEL BLEW OFF WHEN WE CHANGED PITCH AND PWR FOR DSCNT. MAINT PROBABLY DID NOT INSPECT THE PANEL GOOD ENOUGH WHEN THE WORK WAS DONE AT NIGHT. I WAS ON RESERVE AND RECEIVED A XX05 ALL FOR A XC20 SHOW, XC20 PUSH. 2 FORWARD LATCHES WERE UNDONE ON THE OPPOSITE DOOR. IT WAS POSSIBLE I COULD HAVE MISSED THEM. THE OTHER DOOR HAD SCREW FASTENERS AND COULD BE CLOSED WITHOUT KNOWING THE DOOR WAS SECURED.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.