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|
Attributes | |
ACN | 341542 |
Time | |
Date | 199607 |
Day | Wed |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | atc facility : rckh |
State Reference | FO |
Altitude | msl bound lower : 31000 msl bound upper : 31000 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tower : pdx |
Operator | common carrier : air carrier |
Make Model Name | Commercial Fixed Wing |
Operating Under FAR Part | Part 121 |
Flight Phase | cruise other |
Route In Use | enroute airway : rctp |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : flight engineer pilot : atp |
Experience | flight time last 90 days : 105 flight time total : 12000 flight time type : 4000 |
ASRS Report | 341542 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : commercial pilot : instrument |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | aircraft equipment other aircraft equipment : unspecified other flight crewa |
Resolutory Action | none taken : detected after the fact |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | other |
Narrative:
Aircraft was en route from sel to mnl. Time and fuel were normal until about 2 hours 30 mins into the flight. One moment we had 8.1, 8.1, 8.1 (8100 pounds). Not more than 5 mins later, the center fuel gauge was at about 1800 pounds. Fuel gauge integrity was suspect at first, then the boost pump lights illuminated one by one. Entire crew was in agreement that we have a massive leak in #2 tank. We immediately got clearance to begin diversion to rckm, and landed without incident. The reality of the situation was that we had a fuel gauge qty error that didn't reveal itself until the fuel qty in tank #2 was depleted to 1800 pounds.
Original NASA ASRS Text
Title: ACFT EQUIP PROB. FUEL GAUGE ERROR. FLC BELIEVES ACFT HAS FUEL LEAK AND DIVERTS TO NEAR ARPT FOR LNDG. GAUGE ERROR DETECTED ON POST FLT INSPECTION.
Narrative: ACFT WAS ENRTE FROM SEL TO MNL. TIME AND FUEL WERE NORMAL UNTIL ABOUT 2 HRS 30 MINS INTO THE FLT. ONE MOMENT WE HAD 8.1, 8.1, 8.1 (8100 LBS). NOT MORE THAN 5 MINS LATER, THE CTR FUEL GAUGE WAS AT ABOUT 1800 LBS. FUEL GAUGE INTEGRITY WAS SUSPECT AT FIRST, THEN THE BOOST PUMP LIGHTS ILLUMINATED ONE BY ONE. ENTIRE CREW WAS IN AGREEMENT THAT WE HAVE A MASSIVE LEAK IN #2 TANK. WE IMMEDIATELY GOT CLRNC TO BEGIN DIVERSION TO RCKM, AND LANDED WITHOUT INCIDENT. THE REALITY OF THE SIT WAS THAT WE HAD A FUEL GAUGE QTY ERROR THAT DIDN'T REVEAL ITSELF UNTIL THE FUEL QTY IN TANK #2 WAS DEPLETED TO 1800 LBS.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.