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|
Attributes | |
ACN | 344414 |
Time | |
Date | 199608 |
Day | Tue |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : eyw |
State Reference | FL |
Altitude | agl bound lower : 0 agl bound upper : 1000 |
Environment | |
Flight Conditions | VMC |
Light | Night |
Aircraft 1 | |
Controlling Facilities | tower : eyw tower : sdf |
Operator | common carrier : air carrier |
Make Model Name | Commercial Fixed Wing |
Operating Under FAR Part | Part 121 |
Navigation In Use | Other Other |
Flight Phase | climbout : initial other other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | other other : other pilot : cfi pilot : atp |
Experience | flight time last 90 days : 250 flight time total : 2660 flight time type : 275 |
ASRS Report | 344414 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | aircraft equipment other aircraft equipment : unspecified other flight crewa other other : unspecified |
Resolutory Action | flight crew : declared emergency flight crew : rejected takeoff other |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Narrative:
We began our takeoff roll. At approximately 85 KIAS, we received a momentary master warning light and a #2 engine oil pressure warning light. These lights illuminated, then extinguished. At that point we initiated an abort. At the time of the warning lights, all engine gauges for the #2 engine indicated normal. We taxied clear of the active runway and performed a full power run-up with all engine gauges indicating normal. We taxied back for another takeoff. On climb out, at approximately 1000 ft AGL, the #2 engine oil pressure gauge began to fluctuate, but no master warning or #2 engine oil pressure warning lights illuminated. The decision was made to return to key west airport. The on-call mechanic visually inspected the #2 engine but found no problem. 3 quarts of oil were added to the engine. After being signed off by the mechanic, we completed the trip to miami and completed our schedule with that aircraft with no further problems. I feel the airline could offer more operations training to new hires and veteran employees on how to handle the aftermath of an aborted takeoff.
Original NASA ASRS Text
Title: FLC OF AN MDT TURBOPROP COMMUTER RETURNED TO LAND AFTER ONE OF THE ENG'S OIL PRESSURE WAS FLUCTUATING.
Narrative: WE BEGAN OUR TKOF ROLL. AT APPROX 85 KIAS, WE RECEIVED A MOMENTARY MASTER WARNING LIGHT AND A #2 ENG OIL PRESSURE WARNING LIGHT. THESE LIGHTS ILLUMINATED, THEN EXTINGUISHED. AT THAT POINT WE INITIATED AN ABORT. AT THE TIME OF THE WARNING LIGHTS, ALL ENG GAUGES FOR THE #2 ENG INDICATED NORMAL. WE TAXIED CLR OF THE ACTIVE RWY AND PERFORMED A FULL PWR RUN-UP WITH ALL ENG GAUGES INDICATING NORMAL. WE TAXIED BACK FOR ANOTHER TKOF. ON CLBOUT, AT APPROX 1000 FT AGL, THE #2 ENG OIL PRESSURE GAUGE BEGAN TO FLUCTUATE, BUT NO MASTER WARNING OR #2 ENG OIL PRESSURE WARNING LIGHTS ILLUMINATED. THE DECISION WAS MADE TO RETURN TO KEY WEST ARPT. THE ON-CALL MECH VISUALLY INSPECTED THE #2 ENG BUT FOUND NO PROB. 3 QUARTS OF OIL WERE ADDED TO THE ENG. AFTER BEING SIGNED OFF BY THE MECH, WE COMPLETED THE TRIP TO MIAMI AND COMPLETED OUR SCHEDULE WITH THAT ACFT WITH NO FURTHER PROBS. I FEEL THE AIRLINE COULD OFFER MORE OPS TRAINING TO NEW HIRES AND VETERAN EMPLOYEES ON HOW TO HANDLE THE AFTERMATH OF AN ABORTED TKOF.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.