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|
Attributes | |
ACN | 387299 |
Time | |
Date | 199711 |
Day | Thu |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : okc |
State Reference | OK |
Altitude | agl bound lower : 0 agl bound upper : 0 |
Environment | |
Light | Daylight |
Aircraft 1 | |
Operator | common carrier : air carrier |
Make Model Name | Commercial Fixed Wing |
Operating Under FAR Part | Part 121 |
Flight Phase | ground : parked |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : atp |
Experience | flight time last 90 days : 40 flight time total : 5000 flight time type : 500 |
ASRS Report | 387299 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Experience | flight time last 90 days : 191 flight time total : 5540 flight time type : 780 |
ASRS Report | 387298 |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | other other : unspecified |
Resolutory Action | none taken : detected after the fact |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | other |
Narrative:
On nov/thu/97, I served as first officer on aircraft large transport on a flight from ict to okc. The flight had no problems and the aircraft had no discrepancies. After the flight the aircraft was turned over to maintenance in an airworthy condition. On dec/thu/97, I heard from maintenance that the aircraft was left in an unairworthy condition and discrepancies should have been listed in the logbook. This is an untruth. The aircraft was in an airworthy condition. Supplemental information from acn 387298: 6 days later on dec/wed/97, I was notified that large transport was involved in an aborted takeoff.
Original NASA ASRS Text
Title: FLC OF AN ACR CARGO LGT WERE NOTIFIED 6 DAYS AFTER THEIR FLT THAT THE ACFT THEY HAD COMPLETED THEIR SCHEDULED FLT IN HAD ABORTED TKOF APPARENTLY DUE TO EQUIP DISCREPANCIES, AND THAT THE DISCREPANCIES HAD NOT BEEN WRITTEN UP IN THE ACFT LOGBOOK. THE RPTING FLC KNEW NOTHING OF THE DISCREPANCIES SINCE THEY REMEMBERED LEAVING IT IN AN AIRWORTHY CONDITION.
Narrative: ON NOV/THU/97, I SERVED AS FO ON ACFT LGT ON A FLT FROM ICT TO OKC. THE FLT HAD NO PROBS AND THE ACFT HAD NO DISCREPANCIES. AFTER THE FLT THE ACFT WAS TURNED OVER TO MAINT IN AN AIRWORTHY CONDITION. ON DEC/THU/97, I HEARD FROM MAINT THAT THE ACFT WAS LEFT IN AN UNAIRWORTHY CONDITION AND DISCREPANCIES SHOULD HAVE BEEN LISTED IN THE LOGBOOK. THIS IS AN UNTRUTH. THE ACFT WAS IN AN AIRWORTHY CONDITION. SUPPLEMENTAL INFO FROM ACN 387298: 6 DAYS LATER ON DEC/WED/97, I WAS NOTIFIED THAT LGT WAS INVOLVED IN AN ABORTED TKOF.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.