37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 388667 |
Time | |
Date | 199712 |
Day | Wed |
Local Time Of Day | 1801 To 2400 |
Place | |
Locale Reference | atc facility : clt |
State Reference | NC |
Altitude | msl bound lower : 33000 msl bound upper : 33000 |
Environment | |
Flight Conditions | VMC |
Light | Night |
Aircraft 1 | |
Operator | common carrier : air carrier |
Make Model Name | B737-300 |
Operating Under FAR Part | Part 121 |
Navigation In Use | Other |
Flight Phase | cruise other other other |
Route In Use | enroute airway : ztl |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : atp |
Experience | flight time last 90 days : 300 flight time total : 15000 flight time type : 4500 |
ASRS Report | 388667 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Experience | flight time last 90 days : 100 flight time total : 20000 flight time type : 2500 |
ASRS Report | 388663 |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | other flight crewa other other : unspecified cockpit |
Resolutory Action | flight crew : declared emergency other |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Narrative:
While leveling out at FL330, both the captain and I noticed a thumping noise which appeared to come from the forward galley area. This was immediately followed by the cabin altitude climbing at 3000-4000 FPM. We accomplished the excessive cabin altitude checklist. The cabin altitude was uncontrollable. We then immediately accomplished an emergency descent to 10000 ft. We then communicated with the flight attendants and the two deadheading pilots on board as to what they thought might have caused the problem. After evaluating all the information we decided that there was no structural damage and we elected to return to clt. We made an unpressurized landing in clt with no further incident. As we suspected the forward cargo door seal was badly damaged and was the cause of the loss of pressurization.
Original NASA ASRS Text
Title: A B737-300 IN CRUISE AT FL330 DECLARED AN EMER AND DIVERTED DUE TO CABIN DEPRESSURIZATION CAUSED BY A FORWARD CARGO DOOR SEAL DAMAGED AND BLOWN OUT.
Narrative: WHILE LEVELING OUT AT FL330, BOTH THE CAPT AND I NOTICED A THUMPING NOISE WHICH APPEARED TO COME FROM THE FORWARD GALLEY AREA. THIS WAS IMMEDIATELY FOLLOWED BY THE CABIN ALT CLBING AT 3000-4000 FPM. WE ACCOMPLISHED THE EXCESSIVE CABIN ALT CHKLIST. THE CABIN ALT WAS UNCONTROLLABLE. WE THEN IMMEDIATELY ACCOMPLISHED AN EMER DSCNT TO 10000 FT. WE THEN COMMUNICATED WITH THE FLT ATTENDANTS AND THE TWO DEADHEADING PLTS ON BOARD AS TO WHAT THEY THOUGHT MIGHT HAVE CAUSED THE PROB. AFTER EVALUATING ALL THE INFO WE DECIDED THAT THERE WAS NO STRUCTURAL DAMAGE AND WE ELECTED TO RETURN TO CLT. WE MADE AN UNPRESSURIZED LNDG IN CLT WITH NO FURTHER INCIDENT. AS WE SUSPECTED THE FORWARD CARGO DOOR SEAL WAS BADLY DAMAGED AND WAS THE CAUSE OF THE LOSS OF PRESSURIZATION.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.