37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 409379 |
Time | |
Date | 199807 |
Day | Tue |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : anc |
State Reference | AK |
Altitude | agl bound lower : 0 agl bound upper : 0 |
Environment | |
Light | Daylight |
Aircraft 1 | |
Operator | common carrier : air carrier |
Make Model Name | MD-80 Series (DC-9-80) Undifferentiated or Other Model |
Operating Under FAR Part | Part 121 |
Navigation In Use | Other |
Flight Phase | ground : preflight |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : atp |
Experience | flight time last 90 days : 120 flight time total : 3800 flight time type : 250 |
ASRS Report | 409379 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Experience | flight time last 90 days : 200 flight time total : 12600 flight time type : 8000 |
ASRS Report | 409557 |
Events | |
Anomaly | other anomaly other |
Independent Detector | other flight crewa other other : unspecified |
Resolutory Action | other |
Consequence | Other |
Supplementary | |
Air Traffic Incident | other |
Narrative:
MD80 aircraft at anc at the gate, prior to running engine start checklist, APU was previously MEL'ed. A gate start with external air would be required. Aircraft pneumatic system was configured for ventilation when maintenance requested that we motor the left engine to conduct a hydraulic leak check. Since we were only motoring the engine, we did not run the start checklist. The captain opened the xfeeds and started motoring the left engine when the cabin filled with a foul odor. The captain immediately stopped motoring, closed the ventilation switch and shut off the right pack switch. Initially, we thought the fumes may be associated with the potential hydraulic leak that maintenance was looking at on the left engine. The captain decided to deplane the passenger. We then found out that a compressed air bottle was being used as the ground air source. As soon as the fumes entered the aircraft we realized that we inappropriately continued to ventilate while motoring the engine. This allowed contaminated air to enter the aircraft from the compressed air bottle. We obviously made the mistake of continuing to ventilate during the engine motoring. Some contributing factors include an MEL'ed APU, potential hydraulic leak, no knowledge of use of compressed air bottle prior to motoring, no specific procedure for flight crew to do engine motoring for maintenance purposes. Supplemental information from acn 409557: I was unaware that we were going to be starting with a pressurized air bottle that had a history of bad air quality. When the 'motor' sequence started, a foul odor entered the cabin and cockpit. I discontinued the 'motor' and shut off the air conditioning pack. This stopped the bad air flow. The passenger were deplaned in order to ventilate the cabin. Subsequent investigation determined that the source was a contaminated start bottle.
Original NASA ASRS Text
Title: MD80 CREW RPTED COCKPIT AND CABIN FILLED WITH CONTAMINATED AIR.
Narrative: MD80 ACFT AT ANC AT THE GATE, PRIOR TO RUNNING ENG START CHKLIST, APU WAS PREVIOUSLY MEL'ED. A GATE START WITH EXTERNAL AIR WOULD BE REQUIRED. ACFT PNEUMATIC SYS WAS CONFIGURED FOR VENTILATION WHEN MAINT REQUESTED THAT WE MOTOR THE L ENG TO CONDUCT A HYD LEAK CHK. SINCE WE WERE ONLY MOTORING THE ENG, WE DID NOT RUN THE START CHKLIST. THE CAPT OPENED THE XFEEDS AND STARTED MOTORING THE L ENG WHEN THE CABIN FILLED WITH A FOUL ODOR. THE CAPT IMMEDIATELY STOPPED MOTORING, CLOSED THE VENTILATION SWITCH AND SHUT OFF THE R PACK SWITCH. INITIALLY, WE THOUGHT THE FUMES MAY BE ASSOCIATED WITH THE POTENTIAL HYD LEAK THAT MAINT WAS LOOKING AT ON THE L ENG. THE CAPT DECIDED TO DEPLANE THE PAX. WE THEN FOUND OUT THAT A COMPRESSED AIR BOTTLE WAS BEING USED AS THE GND AIR SOURCE. AS SOON AS THE FUMES ENTERED THE ACFT WE REALIZED THAT WE INAPPROPRIATELY CONTINUED TO VENTILATE WHILE MOTORING THE ENG. THIS ALLOWED CONTAMINATED AIR TO ENTER THE ACFT FROM THE COMPRESSED AIR BOTTLE. WE OBVIOUSLY MADE THE MISTAKE OF CONTINUING TO VENTILATE DURING THE ENG MOTORING. SOME CONTRIBUTING FACTORS INCLUDE AN MEL'ED APU, POTENTIAL HYD LEAK, NO KNOWLEDGE OF USE OF COMPRESSED AIR BOTTLE PRIOR TO MOTORING, NO SPECIFIC PROC FOR FLC TO DO ENG MOTORING FOR MAINT PURPOSES. SUPPLEMENTAL INFO FROM ACN 409557: I WAS UNAWARE THAT WE WERE GOING TO BE STARTING WITH A PRESSURIZED AIR BOTTLE THAT HAD A HISTORY OF BAD AIR QUALITY. WHEN THE 'MOTOR' SEQUENCE STARTED, A FOUL ODOR ENTERED THE CABIN AND COCKPIT. I DISCONTINUED THE 'MOTOR' AND SHUT OFF THE AIR CONDITIONING PACK. THIS STOPPED THE BAD AIR FLOW. THE PAX WERE DEPLANED IN ORDER TO VENTILATE THE CABIN. SUBSEQUENT INVESTIGATION DETERMINED THAT THE SOURCE WAS A CONTAMINATED START BOTTLE.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.