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|
Attributes | |
ACN | 413308 |
Time | |
Date | 199809 |
Day | Fri |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | airport : zzz |
State Reference | US |
Altitude | agl bound lower : 0 agl bound upper : 0 |
Environment | |
Light | Daylight |
Aircraft 1 | |
Operator | general aviation : personal |
Make Model Name | M-20 B/C Ranger |
Operating Under FAR Part | Part 91 |
Flight Phase | other |
Flight Plan | None |
Person 1 | |
Affiliation | Other |
Function | other personnel |
Qualification | other other : other |
ASRS Report | 413308 |
Person 2 | |
Affiliation | Other |
Function | other personnel |
Events | |
Anomaly | aircraft equipment problem : critical non adherence : far non adherence : published procedure |
Independent Detector | other other : unspecified cockpit |
Resolutory Action | none taken : detected after the fact |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | other |
Narrative:
At XA30 on sep/xy/98, owner/operator telephoned and stated his belief that during an annual inspection completed jun/yy/98 that a cotter pin securing the throttle linkage was left out resulting in loss of engine power control. Checklists and notes were reviewed and no conclusions could be drawn one way or another. When aircraft was brought to our facility it was in poor condition with several items that were very serious, including unauthorized major alterations performed by person or persons unknown. Callback conversation with reporter revealed the following information: the reporter stated the aircraft had been in service for 2 months when the owner operator reported the linkage problem. The reporter said it appears this owner operator is disgruntled over the annual repair bill and wants to recover a portion of the bill. The reporter said the engine was removed to repair a cracked motor mount and when reinstalled the throttle linkage was adjusted by the shop mechanic and then reinspected by the certified inspector. The reporter stated there is no separate signoff for the throttle linkage adjustment and operational check. The reporter said the FAA has made no contact with the reporter.
Original NASA ASRS Text
Title: A MOONEY MC20C OWNER OPERATOR ADVISED THE RPTR THAT A COTTER PIN SECURING THE THROTTLE LINKAGE WAS OMITTED DURING THE ANNUAL CHK AND CAUSED A LOSS OF PWR.
Narrative: AT XA30 ON SEP/XY/98, OWNER/OPERATOR TELEPHONED AND STATED HIS BELIEF THAT DURING AN ANNUAL INSPECTION COMPLETED JUN/YY/98 THAT A COTTER PIN SECURING THE THROTTLE LINKAGE WAS LEFT OUT RESULTING IN LOSS OF ENG PWR CTL. CHKLISTS AND NOTES WERE REVIEWED AND NO CONCLUSIONS COULD BE DRAWN ONE WAY OR ANOTHER. WHEN ACFT WAS BROUGHT TO OUR FACILITY IT WAS IN POOR CONDITION WITH SEVERAL ITEMS THAT WERE VERY SERIOUS, INCLUDING UNAUTH MAJOR ALTERATIONS PERFORMED BY PERSON OR PERSONS UNKNOWN. CALLBACK CONVERSATION WITH RPTR REVEALED THE FOLLOWING INFO: THE RPTR STATED THE ACFT HAD BEEN IN SVC FOR 2 MONTHS WHEN THE OWNER OPERATOR RPTED THE LINKAGE PROB. THE RPTR SAID IT APPEARS THIS OWNER OPERATOR IS DISGRUNTLED OVER THE ANNUAL REPAIR BILL AND WANTS TO RECOVER A PORTION OF THE BILL. THE RPTR SAID THE ENG WAS REMOVED TO REPAIR A CRACKED MOTOR MOUNT AND WHEN REINSTALLED THE THROTTLE LINKAGE WAS ADJUSTED BY THE SHOP MECH AND THEN REINSPECTED BY THE CERTIFIED INSPECTOR. THE RPTR STATED THERE IS NO SEPARATE SIGNOFF FOR THE THROTTLE LINKAGE ADJUSTMENT AND OPERATIONAL CHK. THE RPTR SAID THE FAA HAS MADE NO CONTACT WITH THE RPTR.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.